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|
Attributes | |
ACN | 263071 |
Time | |
Date | 199402 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : ord |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | descent : approach landing other |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : flight engineer pilot : instrument |
Experience | flight time last 90 days : 110 flight time total : 6000 flight time type : 3000 |
ASRS Report | 263071 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : flight engineer pilot : commercial pilot : atp pilot : cfi |
Experience | flight time last 90 days : 125 flight time total : 15200 flight time type : 4041 |
ASRS Report | 263201 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | other Other |
Narrative:
On final approach to ord, upon putting the gear down on the B-737-100, we had 2 green lights and a red unsafe light on the left main landing gear. A couple of quick checks were unsuccessful and a go around was initiated. We received vector out over lake michigan where we recycled the gear numerous times. We went through the manual gear extension procedure, and a check of the viewing port in the main cabin revealed that the left main gear was jammed only 3 ft out of the wheel well. A few more attempts to recycle the gear were made and also attempts to shake it down were made. At this point, we were down to about 35 mins fuel on board and it was time to prepare for the partial gear up landing. The emergency had been declared earlier when it was discovered that the left main gear was hung up. We went through all abnormal and emergency checklists and the cabin was prepared. The landing was smooth and shutdown of the #1 engine was accomplished just prior to engine contact with the runway. We stopped the aircraft on the centerline of runway 32L. No fire was noted and the fire chief informed us of a small amount of what appeared to be engine oil coming from engine #1. The passenger were taken off the aircraft via stairs and loaded onto busses and taken to the terminal. No injuries to pas or crew, and minor cowl damage only to the #1 engine. So aircraft damage was minor. Supplemental information from acn 263553: while maintenance was in control of a 737-100, wheel chocks were inadvertently placed in the left wheel well and were not removed prior to the next flight. This caused the landing gear on the left side to become jammed in the retracted position. The left main landing gear would not extend and caused aircraft to make a 2 point landing.
Original NASA ASRS Text
Title: MLG UNABLE TO EXTEND L MAIN LNDG GEAR. MAKES EMER LNDG.
Narrative: ON FINAL APCH TO ORD, UPON PUTTING THE GEAR DOWN ON THE B-737-100, WE HAD 2 GREEN LIGHTS AND A RED UNSAFE LIGHT ON THE L MAIN LNDG GEAR. A COUPLE OF QUICK CHKS WERE UNSUCCESSFUL AND A GAR WAS INITIATED. WE RECEIVED VECTOR OUT OVER LAKE MICHIGAN WHERE WE RECYCLED THE GEAR NUMEROUS TIMES. WE WENT THROUGH THE MANUAL GEAR EXTENSION PROC, AND A CHK OF THE VIEWING PORT IN THE MAIN CABIN REVEALED THAT THE L MAIN GEAR WAS JAMMED ONLY 3 FT OUT OF THE WHEEL WELL. A FEW MORE ATTEMPTS TO RECYCLE THE GEAR WERE MADE AND ALSO ATTEMPTS TO SHAKE IT DOWN WERE MADE. AT THIS POINT, WE WERE DOWN TO ABOUT 35 MINS FUEL ON BOARD AND IT WAS TIME TO PREPARE FOR THE PARTIAL GEAR UP LNDG. THE EMER HAD BEEN DECLARED EARLIER WHEN IT WAS DISCOVERED THAT THE L MAIN GEAR WAS HUNG UP. WE WENT THROUGH ALL ABNORMAL AND EMER CHKLISTS AND THE CABIN WAS PREPARED. THE LNDG WAS SMOOTH AND SHUTDOWN OF THE #1 ENG WAS ACCOMPLISHED JUST PRIOR TO ENG CONTACT WITH THE RWY. WE STOPPED THE ACFT ON THE CTRLINE OF RWY 32L. NO FIRE WAS NOTED AND THE FIRE CHIEF INFORMED US OF A SMALL AMOUNT OF WHAT APPEARED TO BE ENG OIL COMING FROM ENG #1. THE PAX WERE TAKEN OFF THE ACFT VIA STAIRS AND LOADED ONTO BUSSES AND TAKEN TO THE TERMINAL. NO INJURIES TO PAS OR CREW, AND MINOR COWL DAMAGE ONLY TO THE #1 ENG. SO ACFT DAMAGE WAS MINOR. SUPPLEMENTAL INFO FROM ACN 263553: WHILE MAINT WAS IN CTL OF A 737-100, WHEEL CHOCKS WERE INADVERTENTLY PLACED IN THE L WHEEL WELL AND WERE NOT REMOVED PRIOR TO THE NEXT FLT. THIS CAUSED THE LNDG GEAR ON THE L SIDE TO BECOME JAMMED IN THE RETRACTED POS. THE L MAIN LNDG GEAR WOULD NOT EXTEND AND CAUSED ACFT TO MAKE A 2 POINT LNDG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.