37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 272222 |
Time | |
Date | 199405 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : boi |
State Reference | ID |
Altitude | msl bound lower : 35000 msl bound upper : 35450 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Controlling Facilities | artcc : zlc tower : las |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Route In Use | enroute : direct enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 100 flight time total : 4913 flight time type : 2709 |
ASRS Report | 272222 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : commercial |
Experience | flight time last 90 days : 150 flight time total : 11000 flight time type : 7000 |
ASRS Report | 272054 |
Events | |
Anomaly | altitude deviation : excursion from assigned altitude non adherence : clearance other anomaly other other spatial deviation |
Independent Detector | other controllera other flight crewa |
Resolutory Action | flight crew : returned to intended course or assigned course flight crew : became reoriented other |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
I made the takeoff from casper, wy. We were cleared to fly a 265 degree heading, proceed direct to boise, identification, before reaching FL350. Approximately 250 NM east of boise, at FL350, we received a 260 degree heading as a course correction. I had the autoplt coupled and made a heading change.I thought I returned the turn knob to the center detent. I was discussing something with the flight engineer and captain -- the next thing I responded to was the captain telling me we were almost to a 180 degree heading and still turning. I immediately turned to a 260 degree heading. We were still corrected back in the correcting turn when center called and queried us on our position. The center did not indicate any near miss or other traffic as a conflict. The only reason that I can think I did this is fatigue. Although this was my first flight and I laid down in time to get plenty of sleep, I didn't get to sleep until about 1 1/2 hours before I had to get up. Both the other crewmembers had been up all night flying, but were in crew rest prior. Supplemental information from acn 272054: a contributing factor to this situation was that we had been flying all night and were all very tired at the time. As the first officer attempted to correct back to the correct heading, he let the aircraft climb 450 ft.
Original NASA ASRS Text
Title: HDG TRACK ALTDEV ALT EXCURSION.
Narrative: I MADE THE TKOF FROM CASPER, WY. WE WERE CLRED TO FLY A 265 DEG HDG, PROCEED DIRECT TO BOISE, ID, BEFORE REACHING FL350. APPROX 250 NM E OF BOISE, AT FL350, WE RECEIVED A 260 DEG HDG AS A COURSE CORRECTION. I HAD THE AUTOPLT COUPLED AND MADE A HDG CHANGE.I THOUGHT I RETURNED THE TURN KNOB TO THE CTR DETENT. I WAS DISCUSSING SOMETHING WITH THE FE AND CAPT -- THE NEXT THING I RESPONDED TO WAS THE CAPT TELLING ME WE WERE ALMOST TO A 180 DEG HDG AND STILL TURNING. I IMMEDIATELY TURNED TO A 260 DEG HDG. WE WERE STILL CORRECTED BACK IN THE CORRECTING TURN WHEN CTR CALLED AND QUERIED US ON OUR POS. THE CTR DID NOT INDICATE ANY NEAR MISS OR OTHER TFC AS A CONFLICT. THE ONLY REASON THAT I CAN THINK I DID THIS IS FATIGUE. ALTHOUGH THIS WAS MY FIRST FLT AND I LAID DOWN IN TIME TO GET PLENTY OF SLEEP, I DIDN'T GET TO SLEEP UNTIL ABOUT 1 1/2 HRS BEFORE I HAD TO GET UP. BOTH THE OTHER CREWMEMBERS HAD BEEN UP ALL NIGHT FLYING, BUT WERE IN CREW REST PRIOR. SUPPLEMENTAL INFO FROM ACN 272054: A CONTRIBUTING FACTOR TO THIS SIT WAS THAT WE HAD BEEN FLYING ALL NIGHT AND WERE ALL VERY TIRED AT THE TIME. AS THE FO ATTEMPTED TO CORRECT BACK TO THE CORRECT HDG, HE LET THE ACFT CLB 450 FT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.