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|
Attributes | |
ACN | 278111 |
Time | |
Date | 199407 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : msy airport : iah |
State Reference | LA |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zhu tower : lax |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | cruise other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 130 flight time total : 14000 flight time type : 50 |
ASRS Report | 278111 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : flight engineer pilot : commercial pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 12000 flight time type : 1800 |
ASRS Report | 278110 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : overcame equipment problem flight crew : declared emergency |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
At cruise altitude atl-iah we got equipment cooling light, went to alternate and tried several times back to normal but got light back, returned to alternate and kept it there. Mins later got dual dc fail light on IRS. Called maintenance control. As we were talking to maintenance control, battery bus showed negative and the battery was discharging. Generators were normal. Anti-skid light came on. We asked maintenance if we should pull battery charger circuit breaker. They said 'yes,' we pulled it. Then we lost N1 and egt's, (both engines). As we were talking, we lost communication #2. WX at msy and WX between us and lft, we decided to continue to iah. We then lost captain's ADI and HSI. Switched his to #2. Tried to switch attitude but lost autoplt. We went back to normal to keep autoplt. We went to flight manual to see what we had or had lost. We then got reverser lights, red gear lights and elevator feel light. We tried to call flight attendants but the call button and PA didn't work. We declared emergency. I flew on autoplt to 2000 ft and then hand flew it. On long final I went back in cabin to verify gear lights. I made normal landing. As we taxied off runway, we smelled smoke. Captain had me get out of my seat and open cabin door since the switch didn't work. We saw thick smoke in cabin. Captain gave order to 'easy vector' out L1, L2 and R2. Nobody was hurt. The smoke was due to packs overheating.
Original NASA ASRS Text
Title: LOSS OF EQUIP COOLING CAUSES A CHAIN REACTION.
Narrative: AT CRUISE ALT ATL-IAH WE GOT EQUIP COOLING LIGHT, WENT TO ALTERNATE AND TRIED SEVERAL TIMES BACK TO NORMAL BUT GOT LIGHT BACK, RETURNED TO ALTERNATE AND KEPT IT THERE. MINS LATER GOT DUAL DC FAIL LIGHT ON IRS. CALLED MAINT CTL. AS WE WERE TALKING TO MAINT CTL, BATTERY BUS SHOWED NEGATIVE AND THE BATTERY WAS DISCHARGING. GENERATORS WERE NORMAL. ANTI-SKID LIGHT CAME ON. WE ASKED MAINT IF WE SHOULD PULL BATTERY CHARGER CIRCUIT BREAKER. THEY SAID 'YES,' WE PULLED IT. THEN WE LOST N1 AND EGT'S, (BOTH ENGS). AS WE WERE TALKING, WE LOST COM #2. WX AT MSY AND WX BTWN US AND LFT, WE DECIDED TO CONTINUE TO IAH. WE THEN LOST CAPT'S ADI AND HSI. SWITCHED HIS TO #2. TRIED TO SWITCH ATTITUDE BUT LOST AUTOPLT. WE WENT BACK TO NORMAL TO KEEP AUTOPLT. WE WENT TO FLT MANUAL TO SEE WHAT WE HAD OR HAD LOST. WE THEN GOT REVERSER LIGHTS, RED GEAR LIGHTS AND ELEVATOR FEEL LIGHT. WE TRIED TO CALL FLT ATTENDANTS BUT THE CALL BUTTON AND PA DIDN'T WORK. WE DECLARED EMER. I FLEW ON AUTOPLT TO 2000 FT AND THEN HAND FLEW IT. ON LONG FINAL I WENT BACK IN CABIN TO VERIFY GEAR LIGHTS. I MADE NORMAL LNDG. AS WE TAXIED OFF RWY, WE SMELLED SMOKE. CAPT HAD ME GET OUT OF MY SEAT AND OPEN CABIN DOOR SINCE THE SWITCH DIDN'T WORK. WE SAW THICK SMOKE IN CABIN. CAPT GAVE ORDER TO 'EASY VECTOR' OUT L1, L2 AND R2. NOBODY WAS HURT. THE SMOKE WAS DUE TO PACKS OVERHEATING.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.