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|
Attributes | |
ACN | 280915 |
Time | |
Date | 199408 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : ack |
State Reference | MA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Cessna 402/402C/B379 Businessliner/Utiliner |
Operating Under FAR Part | Part 135 |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : single pilot |
Qualification | pilot : atp pilot : cfi |
Experience | flight time last 90 days : 180 flight time total : 13700 flight time type : 1050 |
ASRS Report | 280915 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other oversight : supervisor |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure non adherence : far |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : rejected takeoff other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
I aborted a takeoff at nantucket airport on runway 24, due to nosewheel shimmy. I returned to the ramp and off-loaded all passenger. I inspected the aircraft and could find nothing loose or leaking in nosewheel area. I discussed the problem by phone with the chief pilot and we concluded that the weight and crosswind could have set up the nosewheel shimmy in the cessna 402. The chief pilot suggested that I try a second takeoff empty to see if the shimmy was present. I took off without any passenger and had no nosewheel shimmy. Upon reaching hyannis I requested that a mechanic make an inspection of the nosewheel area and the mechanic found that the shimmy dampener had been leaking. He rebuilt the dampener and requested that I write up the problem in the logbook to necessitate him (the mechanic) being called in on a sunday. A detailed inspection by a mechanic should have been done in nantucket and if he had found the dampener to be leaking, the part could have been flown in on our next flight and changed at nantucket. The aircraft then could have been returned to service and actually saved the company money and me some grief.
Original NASA ASRS Text
Title: COMMUTER C-402 TEST FLOWN AND FERRIED WITHOUT PROPER AUTH OR LOG BOOK ENTRIES.
Narrative: I ABORTED A TKOF AT NANTUCKET ARPT ON RWY 24, DUE TO NOSEWHEEL SHIMMY. I RETURNED TO THE RAMP AND OFF-LOADED ALL PAX. I INSPECTED THE ACFT AND COULD FIND NOTHING LOOSE OR LEAKING IN NOSEWHEEL AREA. I DISCUSSED THE PROB BY PHONE WITH THE CHIEF PLT AND WE CONCLUDED THAT THE WT AND XWIND COULD HAVE SET UP THE NOSEWHEEL SHIMMY IN THE CESSNA 402. THE CHIEF PLT SUGGESTED THAT I TRY A SECOND TKOF EMPTY TO SEE IF THE SHIMMY WAS PRESENT. I TOOK OFF WITHOUT ANY PAX AND HAD NO NOSEWHEEL SHIMMY. UPON REACHING HYANNIS I REQUESTED THAT A MECH MAKE AN INSPECTION OF THE NOSEWHEEL AREA AND THE MECH FOUND THAT THE SHIMMY DAMPENER HAD BEEN LEAKING. HE REBUILT THE DAMPENER AND REQUESTED THAT I WRITE UP THE PROB IN THE LOGBOOK TO NECESSITATE HIM (THE MECH) BEING CALLED IN ON A SUNDAY. A DETAILED INSPECTION BY A MECH SHOULD HAVE BEEN DONE IN NANTUCKET AND IF HE HAD FOUND THE DAMPENER TO BE LEAKING, THE PART COULD HAVE BEEN FLOWN IN ON OUR NEXT FLT AND CHANGED AT NANTUCKET. THE ACFT THEN COULD HAVE BEEN RETURNED TO SVC AND ACTUALLY SAVED THE COMPANY MONEY AND ME SOME GRIEF.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.