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|
Attributes | |
ACN | 284884 |
Time | |
Date | 199410 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : mco |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 284884 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | aircraft : equipment problem dissipated flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Airport |
Air Traffic Incident | other |
Situations | |
ATC Facility | other physical facility |
Narrative:
During takeoff from mco nosewheel vibration was excessive takeoff was aborted at very low speed. Northwest problem was analyzed by crew on taxi-in and northwest was tested with a high speed taxi. 2ND takeoff normal. Callback conversation with reporter revealed the following information: reporter was asked how the flight crew had determined that there was just a temperature problem with the nosewheel and that it would be ok for another takeoff. He stated that the crew remembered seeing a 'rut,' similar to a pothole, in the runway just prior to the start of the vibration. They felt that this pothole had instigated the temperature imbal situation and therefore used the high speed taxi test to prove their theory as being correct. Upon arrival at their next stop, bna, the ground crew said the upper portion of the nose strut needed greasing. Not known if that was associated with the vibration at mco. Tower was advised of the 'rut' and reporter said it was repaired at a later date.
Original NASA ASRS Text
Title: TKOF ABORTED WHEN NOSEWHEEL DEVELOPS EXCESSIVE VIBRATION.
Narrative: DURING TKOF FROM MCO NOSEWHEEL VIBRATION WAS EXCESSIVE TKOF WAS ABORTED AT VERY LOW SPD. NW PROB WAS ANALYZED BY CREW ON TAXI-IN AND NW WAS TESTED WITH A HIGH SPD TAXI. 2ND TKOF NORMAL. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: RPTR WAS ASKED HOW THE FLC HAD DETERMINED THAT THERE WAS JUST A TEMP PROB WITH THE NOSEWHEEL AND THAT IT WOULD BE OK FOR ANOTHER TKOF. HE STATED THAT THE CREW REMEMBERED SEEING A 'RUT,' SIMILAR TO A POTHOLE, IN THE RWY JUST PRIOR TO THE START OF THE VIBRATION. THEY FELT THAT THIS POTHOLE HAD INSTIGATED THE TEMP IMBAL SIT AND THEREFORE USED THE HIGH SPD TAXI TEST TO PROVE THEIR THEORY AS BEING CORRECT. UPON ARR AT THEIR NEXT STOP, BNA, THE GND CREW SAID THE UPPER PORTION OF THE NOSE STRUT NEEDED GREASING. NOT KNOWN IF THAT WAS ASSOCIATED WITH THE VIBRATION AT MCO. TWR WAS ADVISED OF THE 'RUT' AND RPTR SAID IT WAS REPAIRED AT A LATER DATE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.