37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 291128 |
Time | |
Date | 199412 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : zbw |
State Reference | MA |
Altitude | msl bound lower : 38000 msl bound upper : 39000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zbw |
Operator | general aviation : corporate |
Make Model Name | Learjet 36 |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : commercial pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 6000 flight time type : 150 |
ASRS Report | 291128 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : less severe altitude deviation : excursion from assigned altitude inflight encounter other non adherence : clearance other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : regained aircraft control flight crew : returned to intended course or assigned course |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
While in a routing climb from FL350 to FL390 in a lear 36A I encountered moderate to severe clear air turbulence. I had just leveled at FL390 and had engaged the altitude hold of the autoplt, the turbulence was encountered at about this time. In the turbulence the autoplt disengaged and consequently we were placed in a nose down position. Our mach number was .78 and with this pitch down began to increase rapidly. In an effort to decrease our rate of descent I gently applied back pressure while decreasing the thrust to flight idle. At this point I immediately encountered aileron activity (buzz) and was forced to release back pressure. Slowly the rate of descent decreased and I was able to regain control. No damage was done to the aircraft, only a shaken flight crew and passenger. Possible ways to prevent this from happening again: cruise at lower mach numbers. In retrospect an emergency should have been declared when I realized that the rate of descent could not be stopped. Total altitude loss was about 1000 ft and recovery to FL390 was made as quickly as possible. In the activity I also neglected to forward the report of turbulence on to ATC which was also my error.
Original NASA ASRS Text
Title: ALT BUST AFTER AUTOPLT TRIPS OFF.
Narrative: WHILE IN A RTING CLB FROM FL350 TO FL390 IN A LEAR 36A I ENCOUNTERED MODERATE TO SEVERE CLR AIR TURB. I HAD JUST LEVELED AT FL390 AND HAD ENGAGED THE ALT HOLD OF THE AUTOPLT, THE TURB WAS ENCOUNTERED AT ABOUT THIS TIME. IN THE TURB THE AUTOPLT DISENGAGED AND CONSEQUENTLY WE WERE PLACED IN A NOSE DOWN POS. OUR MACH NUMBER WAS .78 AND WITH THIS PITCH DOWN BEGAN TO INCREASE RAPIDLY. IN AN EFFORT TO DECREASE OUR RATE OF DSCNT I GENTLY APPLIED BACK PRESSURE WHILE DECREASING THE THRUST TO FLT IDLE. AT THIS POINT I IMMEDIATELY ENCOUNTERED AILERON ACTIVITY (BUZZ) AND WAS FORCED TO RELEASE BACK PRESSURE. SLOWLY THE RATE OF DSCNT DECREASED AND I WAS ABLE TO REGAIN CTL. NO DAMAGE WAS DONE TO THE ACFT, ONLY A SHAKEN FLC AND PAX. POSSIBLE WAYS TO PREVENT THIS FROM HAPPENING AGAIN: CRUISE AT LOWER MACH NUMBERS. IN RETROSPECT AN EMER SHOULD HAVE BEEN DECLARED WHEN I REALIZED THAT THE RATE OF DSCNT COULD NOT BE STOPPED. TOTAL ALT LOSS WAS ABOUT 1000 FT AND RECOVERY TO FL390 WAS MADE AS QUICKLY AS POSSIBLE. IN THE ACTIVITY I ALSO NEGLECTED TO FORWARD THE RPT OF TURB ON TO ATC WHICH WAS ALSO MY ERROR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.