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|
Attributes | |
ACN | 299470 |
Time | |
Date | 199503 |
Day | Mon |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | airport : msp |
State Reference | MN |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 90 flight time total : 13000 flight time type : 7500 |
ASRS Report | 299470 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : rejected takeoff |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
On takeoff roll, noticed controls very stiff. Discontinued takeoff and cleared runway. We then discovered autoplt switch had been inadvertently turned on. Checked system several times and normal takeoff made. Callback conversation with reporter revealed the following information: the reporter flies the md-80 for a major united states air carrier. He does not fly much as he is on reserve. The md-80 autoplt switch is just left of center below the glare shield. When the flight crew had to change from a flex takeoff mode to a non-flex takeoff, the first officer, who is very short, pulled himself forward with his left hand to change some engine parameters. In doing this, he inadvertently engaged the autoplt. The takeoff abort was reported to the air carrier flight department. The captain got a call from his chief pilot within an hour after getting to his layover hotel. Both the captain and first officer got a line check when flying through their home base the next day. The reporter has not heard from the FAA on this. The reporter said that his chief pilot had never heard of this type incident.
Original NASA ASRS Text
Title: TKOF ABORTED.
Narrative: ON TKOF ROLL, NOTICED CTLS VERY STIFF. DISCONTINUED TKOF AND CLRED RWY. WE THEN DISCOVERED AUTOPLT SWITCH HAD BEEN INADVERTENTLY TURNED ON. CHKED SYS SEVERAL TIMES AND NORMAL TKOF MADE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR FLIES THE MD-80 FOR A MAJOR UNITED STATES ACR. HE DOES NOT FLY MUCH AS HE IS ON RESERVE. THE MD-80 AUTOPLT SWITCH IS JUST L OF CTR BELOW THE GLARE SHIELD. WHEN THE FLC HAD TO CHANGE FROM A FLEX TKOF MODE TO A NON-FLEX TKOF, THE FO, WHO IS VERY SHORT, PULLED HIMSELF FORWARD WITH HIS L HAND TO CHANGE SOME ENG PARAMETERS. IN DOING THIS, HE INADVERTENTLY ENGAGED THE AUTOPLT. THE TKOF ABORT WAS RPTED TO THE ACR FLT DEPT. THE CAPT GOT A CALL FROM HIS CHIEF PLT WITHIN AN HR AFTER GETTING TO HIS LAYOVER HOTEL. BOTH THE CAPT AND FO GOT A LINE CHK WHEN FLYING THROUGH THEIR HOME BASE THE NEXT DAY. THE RPTR HAS NOT HEARD FROM THE FAA ON THIS. THE RPTR SAID THAT HIS CHIEF PLT HAD NEVER HEARD OF THIS TYPE INCIDENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.