37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 305701 |
Time | |
Date | 199505 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : lax |
State Reference | CA |
Altitude | msl bound lower : 3000 msl bound upper : 3000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : lax tower : atl |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : initial climbout : intermediate altitude |
Route In Use | departure other departure sid : sid |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : atp pilot : instrument pilot : flight engineer |
Experience | flight time last 90 days : 0 flight time total : 2400 flight time type : 0 |
ASRS Report | 305701 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa other other : unspecified |
Resolutory Action | other |
Consequence | faa : investigated |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Shortly after takeoff we got a call from the flight attendants that there was smoke in the cabin and all of the aft lavatory smoke detectors were going off. We followed procedures in our pilots operating manual but the smoke had not dissipated. I went back to determine type of smoke (flight attendants did not know what electrical smoke smelled like) and to determine severity. It was continuing to remain in the mid to aft cabin area and had an 'oily' smell. We decided to return to lax to have aircraft checked out. During descent the smoke did dissipate. Additionally, when flaps were extended the right side flap indicator tape stopped at 10 degrees but flaps deployed on schedule with no adverse roll inputs. Upon landing at lax we were unable to select reverse thrust. This did not cause a problem due to a low weight and runway length. After shutdown we saw that all 3 circuit breakers had popped on the thrust reversers. It is difficult to say whether they had popped after preflight or if they had been out before. Maintenance fixed all problems, ran all engines, cycled reverse, and fixed flap indicator. We departed 1 1/2 hours later and completed flight without incident. I feel the decision to return to lax was correct. All applicable procedures were followed, and problem appeared to stem from the #3 air-conditioning pack, but this could not be confirmed. The thrust reverser did not have any malfunctions when tested and did not require maintenance. FAA representative had met aircraft at gate at lax but did not comment or have many questions for myself. He did inspect the logbook and go down onto the ramp.
Original NASA ASRS Text
Title: SMOKE APPEARED IN AN ACR'S CABIN SHORTLY AFTER TKOF. THE FLT OPS MANUAL REQUIRED PROCS DIDN'T DISSIPATE THE SMOKE, SO THE FLC CHOSE TO RETURN LAND. A FLAP INDICATOR MALFUNCTIONED DURING DSCNT, AND REVERSE THRUST SELECTION WAS INOP AFTER LNDG. FAA MET THE ACFT.
Narrative: SHORTLY AFTER TKOF WE GOT A CALL FROM THE FLT ATTENDANTS THAT THERE WAS SMOKE IN THE CABIN AND ALL OF THE AFT LAVATORY SMOKE DETECTORS WERE GOING OFF. WE FOLLOWED PROCS IN OUR PLTS OPERATING MANUAL BUT THE SMOKE HAD NOT DISSIPATED. I WENT BACK TO DETERMINE TYPE OF SMOKE (FLT ATTENDANTS DID NOT KNOW WHAT ELECTRICAL SMOKE SMELLED LIKE) AND TO DETERMINE SEVERITY. IT WAS CONTINUING TO REMAIN IN THE MID TO AFT CABIN AREA AND HAD AN 'OILY' SMELL. WE DECIDED TO RETURN TO LAX TO HAVE ACFT CHKED OUT. DURING DSCNT THE SMOKE DID DISSIPATE. ADDITIONALLY, WHEN FLAPS WERE EXTENDED THE R SIDE FLAP INDICATOR TAPE STOPPED AT 10 DEGS BUT FLAPS DEPLOYED ON SCHEDULE WITH NO ADVERSE ROLL INPUTS. UPON LNDG AT LAX WE WERE UNABLE TO SELECT REVERSE THRUST. THIS DID NOT CAUSE A PROB DUE TO A LOW WT AND RWY LENGTH. AFTER SHUTDOWN WE SAW THAT ALL 3 CIRCUIT BREAKERS HAD POPPED ON THE THRUST REVERSERS. IT IS DIFFICULT TO SAY WHETHER THEY HAD POPPED AFTER PREFLT OR IF THEY HAD BEEN OUT BEFORE. MAINT FIXED ALL PROBS, RAN ALL ENGS, CYCLED REVERSE, AND FIXED FLAP INDICATOR. WE DEPARTED 1 1/2 HRS LATER AND COMPLETED FLT WITHOUT INCIDENT. I FEEL THE DECISION TO RETURN TO LAX WAS CORRECT. ALL APPLICABLE PROCS WERE FOLLOWED, AND PROB APPEARED TO STEM FROM THE #3 AIR-CONDITIONING PACK, BUT THIS COULD NOT BE CONFIRMED. THE THRUST REVERSER DID NOT HAVE ANY MALFUNCTIONS WHEN TESTED AND DID NOT REQUIRE MAINT. FAA REPRESENTATIVE HAD MET ACFT AT GATE AT LAX BUT DID NOT COMMENT OR HAVE MANY QUESTIONS FOR MYSELF. HE DID INSPECT THE LOGBOOK AND GO DOWN ONTO THE RAMP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.