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|
Attributes | |
ACN | 317798 |
Time | |
Date | 199510 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : koa |
State Reference | HI |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | ground other : taxi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | other other : other pilot : commercial pilot : instrument pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 10000 flight time type : 2500 |
ASRS Report | 317798 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
While taxiing for takeoff at kona international, flight attendant rang cockpit to inform me that a passenger heard an unusual thumping noise coming from the left hand main landing gear. I did not consider this a problem, and elected to depart. I believed it was safe to continue because: a similar noise reported to me earlier by another company pilot after taxi-in at honolulu international. The company pilot was deadheading in from hilo. I performed a visual inspection and found nothing unusual. The subsequent taxi-out for takeoff to kona was longer than usual and no passenger or cabin crew member reported a thumping sound. Upon arrival at honolulu, I wrote the problem up as a maintenance discrepancy. Maintenance jacked up the left hand main landing gear and re-torqued the wheel assembly. The aircraft was subsequently dispatched. I don't know if maintenance action corrected the problem. Lesson learned here was to get maintenance to look at problem especially at a maintenance base (hnl). Don't know why I didn't write problem up in honolulu. Perhaps it was due to desire to stay on time and complete our last round trip for the day. At a minimum I was not thinking.
Original NASA ASRS Text
Title: DURING TAXI OUT, A PAX RPTED A THUMPING NOISE COMING FROM THE L MAIN LNDG GEAR OF AN MLG.
Narrative: WHILE TAXIING FOR TKOF AT KONA INTL, FLT ATTENDANT RANG COCKPIT TO INFORM ME THAT A PAX HEARD AN UNUSUAL THUMPING NOISE COMING FROM THE L HAND MAIN LNDG GEAR. I DID NOT CONSIDER THIS A PROB, AND ELECTED TO DEPART. I BELIEVED IT WAS SAFE TO CONTINUE BECAUSE: A SIMILAR NOISE RPTED TO ME EARLIER BY ANOTHER COMPANY PLT AFTER TAXI-IN AT HONOLULU INTL. THE COMPANY PLT WAS DEADHEADING IN FROM HILO. I PERFORMED A VISUAL INSPECTION AND FOUND NOTHING UNUSUAL. THE SUBSEQUENT TAXI-OUT FOR TKOF TO KONA WAS LONGER THAN USUAL AND NO PAX OR CABIN CREW MEMBER RPTED A THUMPING SOUND. UPON ARR AT HONOLULU, I WROTE THE PROB UP AS A MAINT DISCREPANCY. MAINT JACKED UP THE L HAND MAIN LNDG GEAR AND RE-TORQUED THE WHEEL ASSEMBLY. THE ACFT WAS SUBSEQUENTLY DISPATCHED. I DON'T KNOW IF MAINT ACTION CORRECTED THE PROB. LESSON LEARNED HERE WAS TO GET MAINT TO LOOK AT PROB ESPECIALLY AT A MAINT BASE (HNL). DON'T KNOW WHY I DIDN'T WRITE PROB UP IN HONOLULU. PERHAPS IT WAS DUE TO DESIRE TO STAY ON TIME AND COMPLETE OUR LAST ROUND TRIP FOR THE DAY. AT A MINIMUM I WAS NOT THINKING.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.