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|
Attributes | |
ACN | 322375 |
Time | |
Date | 199512 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | agl bound lower : 0 agl bound upper : 15000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : cfi |
Experience | flight time last 90 days : 180 flight time total : 3000 |
ASRS Report | 322375 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
We arrived at gate to take flight to memphis. The mechanic informed us on his inspection he found a hydraulic leak in the tail section of the aircraft. The captain went out to see the work in progress. The mechanic informed him he felt the fluid was overfill from the APU engine oil. The captain pointed out to the mechanic that our cockpit gauge indicated slightly above refill. The captain and mechanic both looked at the sight gauge on the reservoir and that confirmed the cockpit gauge. At this point, the captain informed the mechanic he would not accept the aircraft unless he could assure him there was no leak in the system. Total time delay was approximately 1 hour. The mechanic informed us there was no leak and the fluid was replenished. Normal pushback and area departure. At approximately 15000-20000 ft, we noticed hydraulic level was down to the refill level again. We contacted maintenance by voice, and were advised to return to the field and were recommended to have equipment standing by. We advised the first flight attendant to conduct a short preparation of cabin. Overweight landing at 101000 pounds flaps 40 degrees was uneventful.
Original NASA ASRS Text
Title: MLG TAKES DELAY FOR HYD FLUID PROB. DEPARTS AND NOTICES LOW INDICATION FOR HYD FLUID. RETURN LAND.
Narrative: WE ARRIVED AT GATE TO TAKE FLT TO MEMPHIS. THE MECH INFORMED US ON HIS INSPECTION HE FOUND A HYD LEAK IN THE TAIL SECTION OF THE ACFT. THE CAPT WENT OUT TO SEE THE WORK IN PROGRESS. THE MECH INFORMED HIM HE FELT THE FLUID WAS OVERFILL FROM THE APU ENG OIL. THE CAPT POINTED OUT TO THE MECH THAT OUR COCKPIT GAUGE INDICATED SLIGHTLY ABOVE REFILL. THE CAPT AND MECH BOTH LOOKED AT THE SIGHT GAUGE ON THE RESERVOIR AND THAT CONFIRMED THE COCKPIT GAUGE. AT THIS POINT, THE CAPT INFORMED THE MECH HE WOULD NOT ACCEPT THE ACFT UNLESS HE COULD ASSURE HIM THERE WAS NO LEAK IN THE SYS. TOTAL TIME DELAY WAS APPROX 1 HR. THE MECH INFORMED US THERE WAS NO LEAK AND THE FLUID WAS REPLENISHED. NORMAL PUSHBACK AND AREA DEP. AT APPROX 15000-20000 FT, WE NOTICED HYD LEVEL WAS DOWN TO THE REFILL LEVEL AGAIN. WE CONTACTED MAINT BY VOICE, AND WERE ADVISED TO RETURN TO THE FIELD AND WERE RECOMMENDED TO HAVE EQUIP STANDING BY. WE ADVISED THE FIRST FLT ATTENDANT TO CONDUCT A SHORT PREPARATION OF CABIN. OVERWT LNDG AT 101000 LBS FLAPS 40 DEGS WAS UNEVENTFUL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.