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|
Attributes | |
ACN | 324807 |
Time | |
Date | 199512 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : 61b |
State Reference | NV |
Altitude | msl bound lower : 3500 msl bound upper : 3500 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Otter DHC-3 |
Operating Under FAR Part | Part 135 |
Flight Phase | descent : approach descent other other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : atp pilot : commercial pilot : instrument pilot : flight engineer |
Experience | flight time last 90 days : 219 flight time total : 10263 flight time type : 88 |
ASRS Report | 324807 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | faa : investigated other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
On dec/sun/95 at approximately XB30 local, while on a company flight plan from gcn to 61B, flying a dehavilland DH3T aircraft with 10 passenger on board approximately 5 mi northeast of airport 61B at an altitude of approximately 3500 ft MSL on approach. The engine of the 135A aircraft engine had catastrophic failure. While reducing power to approximately 35-30 torque pounds, I heard a sound (a clunk) followed by a grinding sound, strong vibration in rudder pedals, followed by explosion, fire, then smoke. During this time I feathered propeller, condition lever off, ignitors off, emergency oil/fuel shutoff broke off in hand. Fire out, executed an emergency landing to a power line access road 3 mi northeast of 61B. Called mayday twice, second time with no response. Remember noting all engine instruments normal prior. Fuel on board at time 3+ hours, 120 gallons. During landing, aircraft experienced minor damage to right gear, right side nacelle, propeller. Passenger were evacuate/evacuationed with no major injuries. 1 treated for minor. All related company notified. FAA notified. NTSB notified. NASA notified. Note: 3 days prior, I noted a strong vibration in rudder pedals. Notified maintenance. During inspection they found (maintenance) nothing. 2 days prior I noted same vibration in rudder pedals. Noted it at approximately 20-35 torque pounds, momentarily. 1 day prior noted same vibration during power change on second leg of day. All engine instruments normal. On dec/xx/95 took maintenance on test flight, could not reproduce vibration. Engine instrument normal, XA30 local, XB30 local engine failure. Callback conversation with reporter revealed the following information: postflt inspection of aircraft revealed failure of the 5TH stage of the main turbine bearing. Reporter had written that he had felt vibrations in the rudder pedals 2 previous days when flying the same aircraft and reported it to his maintenance facility. Maintenance suspected the vibrations were caused by either an aileron or rudder trim. The day of the engine failure, reporter took a mechanic for a flight, not specifically to check the vibrations, but for pleasure. Reporter says at that time no vibrations were felt at all. However, just a few hours later when on the subject flight the engine failed catastrophically. Having to make a forced landing on a power line access road, some minor aircraft damage was sustained as well as minor passenger injuries. He notified his company head office who in turn notified the FAA and NTSB. The investigation was delayed, but the NTSB was not involved since the FAA labeled it an incident.
Original NASA ASRS Text
Title: ENG FAILURE AND FORCED LNDG. MINOR ACFT DAMAGE AND MINOR PAX INJURIES.
Narrative: ON DEC/SUN/95 AT APPROX XB30 LCL, WHILE ON A COMPANY FLT PLAN FROM GCN TO 61B, FLYING A DEHAVILLAND DH3T ACFT WITH 10 PAX ON BOARD APPROX 5 MI NE OF ARPT 61B AT AN ALT OF APPROX 3500 FT MSL ON APCH. THE ENG OF THE 135A ACFT ENG HAD CATASTROPHIC FAILURE. WHILE REDUCING PWR TO APPROX 35-30 TORQUE LBS, I HEARD A SOUND (A CLUNK) FOLLOWED BY A GRINDING SOUND, STRONG VIBRATION IN RUDDER PEDALS, FOLLOWED BY EXPLOSION, FIRE, THEN SMOKE. DURING THIS TIME I FEATHERED PROP, CONDITION LEVER OFF, IGNITORS OFF, EMER OIL/FUEL SHUTOFF BROKE OFF IN HAND. FIRE OUT, EXECUTED AN EMER LNDG TO A PWR LINE ACCESS ROAD 3 MI NE OF 61B. CALLED MAYDAY TWICE, SECOND TIME WITH NO RESPONSE. REMEMBER NOTING ALL ENG INSTS NORMAL PRIOR. FUEL ON BOARD AT TIME 3+ HRS, 120 GALLONS. DURING LNDG, ACFT EXPERIENCED MINOR DAMAGE TO R GEAR, R SIDE NACELLE, PROP. PAX WERE EVACED WITH NO MAJOR INJURIES. 1 TREATED FOR MINOR. ALL RELATED COMPANY NOTIFIED. FAA NOTIFIED. NTSB NOTIFIED. NASA NOTIFIED. NOTE: 3 DAYS PRIOR, I NOTED A STRONG VIBRATION IN RUDDER PEDALS. NOTIFIED MAINT. DURING INSPECTION THEY FOUND (MAINT) NOTHING. 2 DAYS PRIOR I NOTED SAME VIBRATION IN RUDDER PEDALS. NOTED IT AT APPROX 20-35 TORQUE LBS, MOMENTARILY. 1 DAY PRIOR NOTED SAME VIBRATION DURING PWR CHANGE ON SECOND LEG OF DAY. ALL ENG INSTS NORMAL. ON DEC/XX/95 TOOK MAINT ON TEST FLT, COULD NOT REPRODUCE VIBRATION. ENG INST NORMAL, XA30 LCL, XB30 LCL ENG FAILURE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: POSTFLT INSPECTION OF ACFT REVEALED FAILURE OF THE 5TH STAGE OF THE MAIN TURBINE BEARING. RPTR HAD WRITTEN THAT HE HAD FELT VIBRATIONS IN THE RUDDER PEDALS 2 PREVIOUS DAYS WHEN FLYING THE SAME ACFT AND RPTED IT TO HIS MAINT FACILITY. MAINT SUSPECTED THE VIBRATIONS WERE CAUSED BY EITHER AN AILERON OR RUDDER TRIM. THE DAY OF THE ENG FAILURE, RPTR TOOK A MECH FOR A FLT, NOT SPECIFICALLY TO CHK THE VIBRATIONS, BUT FOR PLEASURE. RPTR SAYS AT THAT TIME NO VIBRATIONS WERE FELT AT ALL. HOWEVER, JUST A FEW HRS LATER WHEN ON THE SUBJECT FLT THE ENG FAILED CATASTROPHICALLY. HAVING TO MAKE A FORCED LNDG ON A PWR LINE ACCESS ROAD, SOME MINOR ACFT DAMAGE WAS SUSTAINED AS WELL AS MINOR PAX INJURIES. HE NOTIFIED HIS COMPANY HEAD OFFICE WHO IN TURN NOTIFIED THE FAA AND NTSB. THE INVESTIGATION WAS DELAYED, BUT THE NTSB WAS NOT INVOLVED SINCE THE FAA LABELED IT AN INCIDENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.