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|
Attributes | |
ACN | 338128 |
Time | |
Date | 199605 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : bil |
State Reference | MT |
Altitude | msl bound lower : 16000 msl bound upper : 16000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : bil |
Operator | common carrier : air taxi |
Make Model Name | King Air 100 A/B |
Operating Under FAR Part | Part 135 |
Flight Phase | climbout : intermediate altitude |
Route In Use | enroute airway : zlc |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 60 flight time total : 4000 flight time type : 140 |
ASRS Report | 338128 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | flight crew : exited penetrated airspace flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
During the pre-takeoff check the pilot turned the start switches on instead of the automatic ignition on the BE10. This gave him the correct indication of ignition lights on. However, it also took the generators off line. The first indication of a problem was a red gear warning light when the gear was retracted. We are now IMC. The gear was cycled because we thought we had a wet uplock switch. This further drained battery power. Within 5 mins we were out of battery power but in VFR on top. We called the company dispatch via cellular phone and told them to call bil tower and cancel our IFR flight plan. This gave us the ability to climb or descend or change route of flight. We flew west toward hln and better VFR WX. Hln tower called my cellular phone and advised of a hole north of hln. We found the hole and descended. Pumped the gear down and landed safely. This problem was caused by the closeness of the switches. The pilot normally flies a BE20. More alertness and differences training were needed. This training is now being given to all of our pilots who fly the king airs.
Original NASA ASRS Text
Title: FLC OF A BEECHCRAFT 100, KING AIR, LOST ALL ELECTRICAL SYS, INCLUDING THE BATTERY SOURCE, IN IMC DUE TO MISMGMNT OF THE START ENG SWITCHES. THE CREW WAS ABLE TO CANCEL IFR VIA A CELLULAR PHONE THROUGH THEIR COMPANY.
Narrative: DURING THE PRE-TKOF CHK THE PLT TURNED THE START SWITCHES ON INSTEAD OF THE AUTO IGNITION ON THE BE10. THIS GAVE HIM THE CORRECT INDICATION OF IGNITION LIGHTS ON. HOWEVER, IT ALSO TOOK THE GENERATORS OFF LINE. THE FIRST INDICATION OF A PROB WAS A RED GEAR WARNING LIGHT WHEN THE GEAR WAS RETRACTED. WE ARE NOW IMC. THE GEAR WAS CYCLED BECAUSE WE THOUGHT WE HAD A WET UPLOCK SWITCH. THIS FURTHER DRAINED BATTERY PWR. WITHIN 5 MINS WE WERE OUT OF BATTERY PWR BUT IN VFR ON TOP. WE CALLED THE COMPANY DISPATCH VIA CELLULAR PHONE AND TOLD THEM TO CALL BIL TWR AND CANCEL OUR IFR FLT PLAN. THIS GAVE US THE ABILITY TO CLB OR DSND OR CHANGE RTE OF FLT. WE FLEW W TOWARD HLN AND BETTER VFR WX. HLN TWR CALLED MY CELLULAR PHONE AND ADVISED OF A HOLE N OF HLN. WE FOUND THE HOLE AND DSNDED. PUMPED THE GEAR DOWN AND LANDED SAFELY. THIS PROB WAS CAUSED BY THE CLOSENESS OF THE SWITCHES. THE PLT NORMALLY FLIES A BE20. MORE ALERTNESS AND DIFFERENCES TRAINING WERE NEEDED. THIS TRAINING IS NOW BEING GIVEN TO ALL OF OUR PLTS WHO FLY THE KING AIRS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.