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|
Attributes | |
ACN | 354625 |
Time | |
Date | 199612 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : zzz tower : rsw |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff other |
Route In Use | departure other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 354625 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
On takeoff out of ZZZ aircraft encountered an airspeed split between the captain's and first officer's airspeed indicators. The split was approximately 40 KTS. Shortly after the discrepancy was encountered it corrected itself. The flight crew elected to return to ZZZ as a precaution, even though airspeed indicator functioned properly for remainder of flight. Upon arrival in ZZZ, maintenance inspected the pitot static ports and found what looked like a piece of plastic melted on the captain's pitot probe. Then maintenance removed the piece of plastic from the side of the pitot probe and did a bite test of the CADC system. The system bite check was good. A research of history in air traffic area 3400 showed no prior discrepancies. It was surmised that a piece of plastic was caught on the pitot tube while the aircraft was either at the gate or on taxi out for takeoff. It melted onto the probe when pitot heat was turned on. After aircraft rotated and began its climb the force of the airflow past the probe must have dislodged the plastic, thus returning the airspeed indication to normal. Loose debris at airport is the suspected cause.
Original NASA ASRS Text
Title: A B737-300 ENCOUNTERED A PLASTIC BAG OR SHEET ON TKOF ROLL WHICH COVERED THE CAPT'S PITOT PROBE CAUSING A 40 KT AIRSPD ERROR. ACFT RETURNED TO THE FIELD.
Narrative: ON TKOF OUT OF ZZZ ACFT ENCOUNTERED AN AIRSPD SPLIT BTWN THE CAPT'S AND FO'S AIRSPD INDICATORS. THE SPLIT WAS APPROX 40 KTS. SHORTLY AFTER THE DISCREPANCY WAS ENCOUNTERED IT CORRECTED ITSELF. THE FLC ELECTED TO RETURN TO ZZZ AS A PRECAUTION, EVEN THOUGH AIRSPD INDICATOR FUNCTIONED PROPERLY FOR REMAINDER OF FLT. UPON ARR IN ZZZ, MAINT INSPECTED THE PITOT STATIC PORTS AND FOUND WHAT LOOKED LIKE A PIECE OF PLASTIC MELTED ON THE CAPT'S PITOT PROBE. THEN MAINT REMOVED THE PIECE OF PLASTIC FROM THE SIDE OF THE PITOT PROBE AND DID A BITE TEST OF THE CADC SYS. THE SYS BITE CHK WAS GOOD. A RESEARCH OF HISTORY IN ATA 3400 SHOWED NO PRIOR DISCREPANCIES. IT WAS SURMISED THAT A PIECE OF PLASTIC WAS CAUGHT ON THE PITOT TUBE WHILE THE ACFT WAS EITHER AT THE GATE OR ON TAXI OUT FOR TKOF. IT MELTED ONTO THE PROBE WHEN PITOT HEAT WAS TURNED ON. AFTER ACFT ROTATED AND BEGAN ITS CLB THE FORCE OF THE AIRFLOW PAST THE PROBE MUST HAVE DISLODGED THE PLASTIC, THUS RETURNING THE AIRSPD INDICATION TO NORMAL. LOOSE DEBRIS AT ARPT IS THE SUSPECTED CAUSE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.