Narrative:

During the attempted takeoff, at vr, the aircraft would not respond to my flight control inputs and did not rotate. Therefore, I aborted the takeoff. The aircraft exited the end of the runway stopping approximately 20 ft into the grass. There was no damage to the aircraft and no injuries. Callback conversation with the reporter revealed the following: the control problem was caused by a faulty potentiometer that directed the elevator trim to go full nose down. The FAA investigated this and called it an incident. The reporter is now flying for a major air carrier.

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Original NASA ASRS Text

Title: A LEAR 24 ATX CARGO PLT HAD A TKOF ABORTED DUE TO A FLT CTL PROB.

Narrative: DURING THE ATTEMPTED TKOF, AT VR, THE ACFT WOULD NOT RESPOND TO MY FLT CTL INPUTS AND DID NOT ROTATE. THEREFORE, I ABORTED THE TKOF. THE ACFT EXITED THE END OF THE RWY STOPPING APPROX 20 FT INTO THE GRASS. THERE WAS NO DAMAGE TO THE ACFT AND NO INJURIES. CALLBACK CONVERSATION WITH THE RPTR REVEALED THE FOLLOWING: THE CTL PROBLEM WAS CAUSED BY A FAULTY POTENTIOMETER THAT DIRECTED THE ELEVATOR TRIM TO GO FULL NOSE DOWN. THE FAA INVESTIGATED THIS AND CALLED IT AN INCIDENT. THE RPTR IS NOW FLYING FOR A MAJOR ACR.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.