37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 356254 |
Time | |
Date | 199612 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : orl |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Learjet 24 |
Operating Under FAR Part | Part 135 |
Flight Phase | climbout : takeoff other other |
Flight Plan | IFR |
Aircraft 2 | |
Make Model Name | Learjet 24 |
Operating Under FAR Part | Part 135 |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp pilot : instrument |
Experience | flight time last 90 days : 150 flight time total : 3500 flight time type : 500 |
ASRS Report | 356254 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical conflict : ground critical other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency flight crew : rejected takeoff |
Consequence | faa : investigated Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
During the attempted takeoff, at vr, the aircraft would not respond to my flight control inputs and did not rotate. Therefore, I aborted the takeoff. The aircraft exited the end of the runway stopping approximately 20 ft into the grass. There was no damage to the aircraft and no injuries. Callback conversation with the reporter revealed the following: the control problem was caused by a faulty potentiometer that directed the elevator trim to go full nose down. The FAA investigated this and called it an incident. The reporter is now flying for a major air carrier.
Original NASA ASRS Text
Title: A LEAR 24 ATX CARGO PLT HAD A TKOF ABORTED DUE TO A FLT CTL PROB.
Narrative: DURING THE ATTEMPTED TKOF, AT VR, THE ACFT WOULD NOT RESPOND TO MY FLT CTL INPUTS AND DID NOT ROTATE. THEREFORE, I ABORTED THE TKOF. THE ACFT EXITED THE END OF THE RWY STOPPING APPROX 20 FT INTO THE GRASS. THERE WAS NO DAMAGE TO THE ACFT AND NO INJURIES. CALLBACK CONVERSATION WITH THE RPTR REVEALED THE FOLLOWING: THE CTL PROBLEM WAS CAUSED BY A FAULTY POTENTIOMETER THAT DIRECTED THE ELEVATOR TRIM TO GO FULL NOSE DOWN. THE FAA INVESTIGATED THIS AND CALLED IT AN INCIDENT. THE RPTR IS NOW FLYING FOR A MAJOR ACR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.