37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 357081 |
Time | |
Date | 199612 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | A320 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 357081 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure non adherence : far other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
In sum: mechanics relieved the earlier mechanics working on a static inverter test that had failed. Several parts were replaced to no avail. After the job was turned over the same system was reset (but would not reset and pass the test) several times for the mechanics. Miraculously the system was reset and dispatched by the mechanics that relieved the reporter. The aircraft failed to test at the next #2 service check. Clearly the desire to get rid of this problem without proper maintenance action caused this aircraft to fly without a properly functioning static inverter system for several days! As previously stated every attempt was made to reset thrust and reverser units in the east&east compartment. But as soon as a static inverter test was attempted, it failed. The reporter alleges that the tests were never redone after the thrust reverser units were reset.
Original NASA ASRS Text
Title: AN AIRBUS 320-232 WAS DISPATCHED WITH THE STATIC INVERTER SYS FAILING THE SYS TEST.
Narrative: IN SUM: MECHS RELIEVED THE EARLIER MECHS WORKING ON A STATIC INVERTER TEST THAT HAD FAILED. SEVERAL PARTS WERE REPLACED TO NO AVAIL. AFTER THE JOB WAS TURNED OVER THE SAME SYS WAS RESET (BUT WOULD NOT RESET AND PASS THE TEST) SEVERAL TIMES FOR THE MECHS. MIRACULOUSLY THE SYS WAS RESET AND DISPATCHED BY THE MECHS THAT RELIEVED THE RPTR. THE ACFT FAILED TO TEST AT THE NEXT #2 SVC CHK. CLRLY THE DESIRE TO GET RID OF THIS PROB WITHOUT PROPER MAINT ACTION CAUSED THIS ACFT TO FLY WITHOUT A PROPERLY FUNCTIONING STATIC INVERTER SYS FOR SEVERAL DAYS! AS PREVIOUSLY STATED EVERY ATTEMPT WAS MADE TO RESET THRUST AND REVERSER UNITS IN THE E&E COMPARTMENT. BUT AS SOON AS A STATIC INVERTER TEST WAS ATTEMPTED, IT FAILED. THE RPTR ALLEGES THAT THE TESTS WERE NEVER REDONE AFTER THE THRUST REVERSER UNITS WERE RESET.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.