37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 362705 |
Time | |
Date | 199703 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : msp |
State Reference | MN |
Altitude | msl bound lower : 8000 msl bound upper : 8000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : msp |
Operator | common carrier : air carrier |
Make Model Name | DC-9 10 |
Operating Under FAR Part | Part 121 |
Flight Phase | descent : approach |
Route In Use | arrival other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain |
Qualification | pilot : atp pilot : flight engineer pilot : instrument pilot : cfi |
Experience | flight time last 90 days : 150 flight time total : 12000 flight time type : 2800 |
ASRS Report | 362705 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Air Traffic Incident | other |
Narrative:
In sum: on approach to msp the left air-conditioning electrical bus failed. Had off lights on xtie lockout, left generator, left air-conditioning bus, and pitot/stall warning heater. First officer was flying and we were on approach control descending to 8000 ft. We asked approach control for vectors so we could solve our electrical problem. The first officer flew the aircraft while I worked the cockpit operating manual procedures to restore power back to the left air-conditioning bus. APU power was switched to the left air-conditioning bus to restore power. Returned to msp for landing without further incident. Callback conversation with reporter revealed the following information: airplane was on descent about 8000 ft when pitot heat light came on with generator off light. Noticed generator voltage was below limits. The APU which was running was switched on to power the left bus. Went through cockpit operating procedures and proceeded to land. Maintenance replaced the left engine constant speed drive as corrective action.
Original NASA ASRS Text
Title: ON DSCNT A DC9-10 LOST ELECTRICAL PWR TO THE L BUS. APU SWITCHED TO PWR L BUS.
Narrative: IN SUM: ON APCH TO MSP THE L AIR-CONDITIONING ELECTRICAL BUS FAILED. HAD OFF LIGHTS ON XTIE LOCKOUT, L GENERATOR, LEFT AIR-CONDITIONING BUS, AND PITOT/STALL WARNING HEATER. FO WAS FLYING AND WE WERE ON APCH CTL DSNDING TO 8000 FT. WE ASKED APCH CTL FOR VECTORS SO WE COULD SOLVE OUR ELECTRICAL PROB. THE FO FLEW THE ACFT WHILE I WORKED THE COCKPIT OPERATING MANUAL PROCS TO RESTORE PWR BACK TO THE L AIR-CONDITIONING BUS. APU PWR WAS SWITCHED TO THE L AIR-CONDITIONING BUS TO RESTORE PWR. RETURNED TO MSP FOR LNDG WITHOUT FURTHER INCIDENT. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: AIRPLANE WAS ON DSCNT ABOUT 8000 FT WHEN PITOT HEAT LIGHT CAME ON WITH GENERATOR OFF LIGHT. NOTICED GENERATOR VOLTAGE WAS BELOW LIMITS. THE APU WHICH WAS RUNNING WAS SWITCHED ON TO PWR THE L BUS. WENT THROUGH COCKPIT OPERATING PROCS AND PROCEEDED TO LAND. MAINT REPLACED THE L ENG CONSTANT SPD DRIVE AS CORRECTIVE ACTION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.