37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 363761 |
Time | |
Date | 199703 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : cha |
State Reference | TN |
Altitude | msl bound lower : 10000 msl bound upper : 10000 |
Environment | |
Flight Conditions | IMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : cha tracon : rme |
Operator | common carrier : air carrier |
Make Model Name | F27 (Fokker BV) |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : commercial pilot : atp pilot : instrument |
Experience | flight time last 90 days : 100 flight time total : 16500 flight time type : 700 |
ASRS Report | 363761 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
In sum: about 30 NM west of chattanooga we smelled fuel. Soon discovered through high fuel flow and low fuel pressure and visual inspection that fuel was streaming from #1 nacelle. We descended from 10000 ft and returned for landing at cha after receiving clearance and declaring emergency. We elected not to feather #1 engine due to windshear and turbulence reported on final approach. Uneventful landing and engine shutdown. There is no written procedure for this problem. I did not perform the ground emergency check but shut down the engine normally. Callback conversation with reporter revealed the following information: aircraft was a foker F27 and had no previous history of fuel leakage on #1 engine. The corrective maintenance action was the replacement of the #1 engine high pressure fuel hose. The reporter was not contacted by the FAA.
Original NASA ASRS Text
Title: A FOKER F27 MADE AN EMER LNDG DUE TO FUEL LEAKING FROM #1 ENG NACELLE.
Narrative: IN SUM: ABOUT 30 NM W OF CHATTANOOGA WE SMELLED FUEL. SOON DISCOVERED THROUGH HIGH FUEL FLOW AND LOW FUEL PRESSURE AND VISUAL INSPECTION THAT FUEL WAS STREAMING FROM #1 NACELLE. WE DSNDED FROM 10000 FT AND RETURNED FOR LNDG AT CHA AFTER RECEIVING CLRNC AND DECLARING EMER. WE ELECTED NOT TO FEATHER #1 ENG DUE TO WINDSHEAR AND TURB RPTED ON FINAL APCH. UNEVENTFUL LNDG AND ENG SHUTDOWN. THERE IS NO WRITTEN PROC FOR THIS PROB. I DID NOT PERFORM THE GND EMER CHK BUT SHUT DOWN THE ENG NORMALLY. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: ACFT WAS A FOKER F27 AND HAD NO PREVIOUS HISTORY OF FUEL LEAKAGE ON #1 ENG. THE CORRECTIVE MAINT ACTION WAS THE REPLACEMENT OF THE #1 ENG HIGH PRESSURE FUEL HOSE. THE RPTR WAS NOT CONTACTED BY THE FAA.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.