37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 366376 |
Time | |
Date | 199704 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : azo |
State Reference | MI |
Altitude | msl bound lower : 4000 msl bound upper : 10000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : azo |
Operator | common carrier : air taxi |
Make Model Name | King Air 100 A/B |
Operating Under FAR Part | Part 135 |
Flight Phase | cruise other descent : approach descent other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : commercial |
Experience | flight time last 90 days : 70 flight time total : 1400 flight time type : 200 |
ASRS Report | 366376 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : regained aircraft control flight crew : returned to intended course or assigned course flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
When leveling at 10000 ft, we had an unscheduled autoplt and trim runaway. Approximately 7 degrees pitch up, followed immediately by a 10 degree pitch down. Upon disabling autoplt, the trim ran away, causing a continuous pitch down. Aircraft was recovered at 4000 ft MSL without autoplt or trim working. Landing completed at azo.
Original NASA ASRS Text
Title: A BE10 HAS AN UNSCHEDULED AUTOPLT AND TRIM RUNAWAY. AFTER A 7 DEG PITCH UP, THEN A 10 DEG PITCH DOWN, THE ACFT MADE A SAFE LNDG AT AZO.
Narrative: WHEN LEVELING AT 10000 FT, WE HAD AN UNSCHEDULED AUTOPLT AND TRIM RUNAWAY. APPROX 7 DEGS PITCH UP, FOLLOWED IMMEDIATELY BY A 10 DEG PITCH DOWN. UPON DISABLING AUTOPLT, THE TRIM RAN AWAY, CAUSING A CONTINUOUS PITCH DOWN. ACFT WAS RECOVERED AT 4000 FT MSL WITHOUT AUTOPLT OR TRIM WORKING. LNDG COMPLETED AT AZO.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.