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|
Attributes | |
ACN | 368890 |
Time | |
Date | 199705 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | msl bound lower : 4000 msl bound upper : 4000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : ord |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | descent : approach landing : go around |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 368890 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
ASRS Report | 368889 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | faa : reviewed incident with flight crew |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Twice during flight we experienced long periods of silence when using #2 VHF radio. When contact re-established ATC informed us that it appeared we had a stuck microphone. All microphone buttons checked normal. We suspected a bad #2 radio transmitter so we started using #1 radio. Operations normal until turning base leg on ILS to runway 22R at ord. With captain transmitting on #1 radio we started receiving only static. Same on #2 radio. Made turn inbound on localizer in IMC conditions. Maintained altitude until we heard approach clear us for visual if field in sight. Unable to contact tower due to static. First officer was trying contact on #2 radio and so was trying on #1 radio with no luck. Broke out of overcast too high/close for safe landing and executed miss. Finally contacted tower and switched approach. Captain disconnected his microphone cord from console and communications became normal. Uneventful approach ldng. Maintenance suspects bad mini amp in captain microphone causing open circuit. Called approach control upon arrival to explain what happened to supervisor. We were told that at no time did any traffic conflict exist.
Original NASA ASRS Text
Title: B727 ACFT ON APCH WAS UNABLE TO COMMUNICATE WITH APCH CTLR OR TWR DUE TO BAD #1 AND #2 RADIOS. GAR WAS EXECUTED AND CAPT DISCONNECTED HIS MIKE CORD WHICH CLRED UP THE RADIO PROB.
Narrative: TWICE DURING FLT WE EXPERIENCED LONG PERIODS OF SILENCE WHEN USING #2 VHF RADIO. WHEN CONTACT RE-ESTABLISHED ATC INFORMED US THAT IT APPEARED WE HAD A STUCK MIKE. ALL MIKE BUTTONS CHKED NORMAL. WE SUSPECTED A BAD #2 RADIO XMITTER SO WE STARTED USING #1 RADIO. OPS NORMAL UNTIL TURNING BASE LEG ON ILS TO RWY 22R AT ORD. WITH CAPT XMITTING ON #1 RADIO WE STARTED RECEIVING ONLY STATIC. SAME ON #2 RADIO. MADE TURN INBOUND ON LOC IN IMC CONDITIONS. MAINTAINED ALT UNTIL WE HEARD APCH CLR US FOR VISUAL IF FIELD IN SIGHT. UNABLE TO CONTACT TWR DUE TO STATIC. FO WAS TRYING CONTACT ON #2 RADIO AND SO WAS TRYING ON #1 RADIO WITH NO LUCK. BROKE OUT OF OVCST TOO HIGH/CLOSE FOR SAFE LNDG AND EXECUTED MISS. FINALLY CONTACTED TWR AND SWITCHED APCH. CAPT DISCONNECTED HIS MIKE CORD FROM CONSOLE AND COMS BECAME NORMAL. UNEVENTFUL APCH LDNG. MAINT SUSPECTS BAD MINI AMP IN CAPT MIKE CAUSING OPEN CIRCUIT. CALLED APCH CTL UPON ARR TO EXPLAIN WHAT HAPPENED TO SUPVR. WE WERE TOLD THAT AT NO TIME DID ANY TFC CONFLICT EXIST.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.