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|
Attributes | |
ACN | 387930 |
Time | |
Date | 199711 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : bos |
State Reference | MA |
Altitude | msl bound lower : 10000 msl bound upper : 10000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Beech 1900 |
Operating Under FAR Part | Part 135 |
Navigation In Use | Other Other |
Flight Phase | cruise other descent other |
Route In Use | enroute airway : bos |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 120 flight time total : 4000 flight time type : 1500 |
ASRS Report | 387930 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 80 flight time total : 4500 flight time type : 1400 |
ASRS Report | 386921 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | faa : investigated Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
We started our initial descent into bos. Low oil pressure light illuminated. The oil pressure was in yellow arc. We then reduced power. Oil pressure continued to go down. We consulted checklist and performed engine failure in-flight checks and other required checks. Landing was uneventful. Mechanics later determined an o-ring failed on the #2 engine.
Original NASA ASRS Text
Title: FLC OF A BEECH 1900 AIRLINER (BE02) SHUT DOWN THE R ENG DUE TO LOW OIL PRESSURE. EMER WAS DECLARED AND ATC GAVE PRIORITY HANDLING TO THEIR DEST WHERE THE FLT TERMINATED. THE CAUSE OF THE ENG PROB WAS DETERMINED TO BE A FAILED O-RING.
Narrative: WE STARTED OUR INITIAL DSCNT INTO BOS. LOW OIL PRESSURE LIGHT ILLUMINATED. THE OIL PRESSURE WAS IN YELLOW ARC. WE THEN REDUCED PWR. OIL PRESSURE CONTINUED TO GO DOWN. WE CONSULTED CHKLIST AND PERFORMED ENG FAILURE INFLT CHKS AND OTHER REQUIRED CHKS. LNDG WAS UNEVENTFUL. MECHS LATER DETERMINED AN O-RING FAILED ON THE #2 ENG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.