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|
Attributes | |
ACN | 391922 |
Time | |
Date | 199801 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Twin Beech 18 |
Operating Under FAR Part | Part 135 |
Flight Phase | other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 391922 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure non adherence : far other anomaly other |
Independent Detector | other flight crewa other other : unspecified cockpit |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
The aircraft was in-flight when flight crew noticed no engine response to power lever setting. Engine was shut down and aircraft landed safely. Aircraft shut down on runway (remaining engine) and was towed off the runway. On inspection, bolt found missing from throttle linkage to fuel control. Last maintenance performed was aircraft inspection where the bolt was removed for inspection. It was concluded bolt was not safetied properly and thus vibrated out. On discussion by shift supervisors it was decided that inspections had been run poorly by passing work from one shift to another. As a result some work didn't get inspected, thus presenting a significant safety hazard. Actions taken to prevent this from happening again are the stressing of the 2 man maintenance concept. Everything is looked at twice and work was no longer passed off to the next shift for completion, but were required to be completed and inspected before the shift was dismissed for the day. Longer, more complex tasks, requiring more time were completed the following day. Also, the rush from operations was looked at and less emphasis on speed and more attention to detail and quality were stressed.
Original NASA ASRS Text
Title: A BEECH 18 INFLT DECLARED AN EMER AND DIVERTED WITH 1 ENG SHUT DOWN DUE TO NO PWR LEVER RESPONSE CAUSED BY A BOLT VIBRATING OUT OF THE FUEL CTL LINKAGE.
Narrative: THE ACFT WAS INFLT WHEN FLC NOTICED NO ENG RESPONSE TO PWR LEVER SETTING. ENG WAS SHUT DOWN AND ACFT LANDED SAFELY. ACFT SHUT DOWN ON RWY (REMAINING ENG) AND WAS TOWED OFF THE RWY. ON INSPECTION, BOLT FOUND MISSING FROM THROTTLE LINKAGE TO FUEL CTL. LAST MAINT PERFORMED WAS ACFT INSPECTION WHERE THE BOLT WAS REMOVED FOR INSPECTION. IT WAS CONCLUDED BOLT WAS NOT SAFETIED PROPERLY AND THUS VIBRATED OUT. ON DISCUSSION BY SHIFT SUPVRS IT WAS DECIDED THAT INSPECTIONS HAD BEEN RUN POORLY BY PASSING WORK FROM ONE SHIFT TO ANOTHER. AS A RESULT SOME WORK DIDN'T GET INSPECTED, THUS PRESENTING A SIGNIFICANT SAFETY HAZARD. ACTIONS TAKEN TO PREVENT THIS FROM HAPPENING AGAIN ARE THE STRESSING OF THE 2 MAN MAINT CONCEPT. EVERYTHING IS LOOKED AT TWICE AND WORK WAS NO LONGER PASSED OFF TO THE NEXT SHIFT FOR COMPLETION, BUT WERE REQUIRED TO BE COMPLETED AND INSPECTED BEFORE THE SHIFT WAS DISMISSED FOR THE DAY. LONGER, MORE COMPLEX TASKS, REQUIRING MORE TIME WERE COMPLETED THE FOLLOWING DAY. ALSO, THE RUSH FROM OPERATIONS WAS LOOKED AT AND LESS EMPHASIS ON SPEED AND MORE ATTENTION TO DETAIL AND QUALITY WERE STRESSED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.