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|
Attributes | |
ACN | 394648 |
Time | |
Date | 199802 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : sju |
State Reference | PR |
Altitude | msl bound lower : 5000 msl bound upper : 5000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : tjzs |
Operator | common carrier : air carrier |
Make Model Name | B727-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude climbout : takeoff ground : preflight |
Route In Use | enroute : other oceanic enroute : atlantic |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 97 flight time total : 14000 flight time type : 11000 |
ASRS Report | 394648 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | none taken : anomaly accepted other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation other |
Narrative:
#3 fire warning sounded and light came on. Silenced bell and retarded throttle. Light went out. Did not shut down engine, restored power, all indications normal. Continued to sju. Had maintenance check engine and found no problems. No logbook entry was made. Departed sju, on climb out problem re-occurred. Retarded throttle and light went out. After approximately 1 min restored power, all temperatures and pressures were normal. Continued to destination. I felt there was a duct leak and was no threat to safety. On third takeoff there were no warnings and engine functioned normally. Upon return to base a log item was made and corrective action was taken. A small crack in a duct was found and repaired.
Original NASA ASRS Text
Title: A B727-200 EXPERIENCES A FIRE WARNING AND LIGHT ON #3 ENG OUT OF MIA. FLT CONTINUED TO SJU AFTER WARNING CEASED WITH THROTTLE REDUCTION AND RESTORATION. MALFUNCTION WAS NOT WRITTEN UP IN LOGBOOK. OCCURRED AGAIN OUT OF SJU BUT NOT THE LEG AFTER. FINALLY, BACK IN MIA, PIC WRITES UP ANOMALY IN LOGBOOK. ACFT FOUND TO HAVE A MINOR RUPTURED DUCT.
Narrative: #3 FIRE WARNING SOUNDED AND LIGHT CAME ON. SILENCED BELL AND RETARDED THROTTLE. LIGHT WENT OUT. DID NOT SHUT DOWN ENG, RESTORED PWR, ALL INDICATIONS NORMAL. CONTINUED TO SJU. HAD MAINT CHK ENG AND FOUND NO PROBS. NO LOGBOOK ENTRY WAS MADE. DEPARTED SJU, ON CLBOUT PROB RE-OCCURRED. RETARDED THROTTLE AND LIGHT WENT OUT. AFTER APPROX 1 MIN RESTORED PWR, ALL TEMPS AND PRESSURES WERE NORMAL. CONTINUED TO DEST. I FELT THERE WAS A DUCT LEAK AND WAS NO THREAT TO SAFETY. ON THIRD TKOF THERE WERE NO WARNINGS AND ENG FUNCTIONED NORMALLY. UPON RETURN TO BASE A LOG ITEM WAS MADE AND CORRECTIVE ACTION WAS TAKEN. A SMALL CRACK IN A DUCT WAS FOUND AND REPAIRED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.