Narrative:

#3 fire warning sounded and light came on. Silenced bell and retarded throttle. Light went out. Did not shut down engine, restored power, all indications normal. Continued to sju. Had maintenance check engine and found no problems. No logbook entry was made. Departed sju, on climb out problem re-occurred. Retarded throttle and light went out. After approximately 1 min restored power, all temperatures and pressures were normal. Continued to destination. I felt there was a duct leak and was no threat to safety. On third takeoff there were no warnings and engine functioned normally. Upon return to base a log item was made and corrective action was taken. A small crack in a duct was found and repaired.

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Original NASA ASRS Text

Title: A B727-200 EXPERIENCES A FIRE WARNING AND LIGHT ON #3 ENG OUT OF MIA. FLT CONTINUED TO SJU AFTER WARNING CEASED WITH THROTTLE REDUCTION AND RESTORATION. MALFUNCTION WAS NOT WRITTEN UP IN LOGBOOK. OCCURRED AGAIN OUT OF SJU BUT NOT THE LEG AFTER. FINALLY, BACK IN MIA, PIC WRITES UP ANOMALY IN LOGBOOK. ACFT FOUND TO HAVE A MINOR RUPTURED DUCT.

Narrative: #3 FIRE WARNING SOUNDED AND LIGHT CAME ON. SILENCED BELL AND RETARDED THROTTLE. LIGHT WENT OUT. DID NOT SHUT DOWN ENG, RESTORED PWR, ALL INDICATIONS NORMAL. CONTINUED TO SJU. HAD MAINT CHK ENG AND FOUND NO PROBS. NO LOGBOOK ENTRY WAS MADE. DEPARTED SJU, ON CLBOUT PROB RE-OCCURRED. RETARDED THROTTLE AND LIGHT WENT OUT. AFTER APPROX 1 MIN RESTORED PWR, ALL TEMPS AND PRESSURES WERE NORMAL. CONTINUED TO DEST. I FELT THERE WAS A DUCT LEAK AND WAS NO THREAT TO SAFETY. ON THIRD TKOF THERE WERE NO WARNINGS AND ENG FUNCTIONED NORMALLY. UPON RETURN TO BASE A LOG ITEM WAS MADE AND CORRECTIVE ACTION WAS TAKEN. A SMALL CRACK IN A DUCT WAS FOUND AND REPAIRED.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.