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|
Attributes | |
ACN | 403350 |
Time | |
Date | 199805 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : lyh |
State Reference | VA |
Altitude | msl bound lower : 16000 msl bound upper : 16000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : bos |
Operator | other |
Make Model Name | Super King Air 300 |
Operating Under FAR Part | Part 91 |
Navigation In Use | Other |
Flight Phase | cruise other |
Route In Use | arrival star : star enroute airway : zdc |
Flight Plan | IFR |
Aircraft 2 | |
Make Model Name | Super King Air 300 |
Operating Under FAR Part | Part 91 |
Person 1 | |
Affiliation | government : faa |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 4900 flight time type : 2600 |
ASRS Report | 403350 |
Person 2 | |
Affiliation | government : faa |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | non adherence : clearance other spatial deviation |
Independent Detector | other controllera |
Resolutory Action | flight crew : became reoriented flight crew : returned to intended course or assigned course |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
The crew was en route to greensboro, nc, via lyh VORTAC and the henby STAR. We were discussing the problems we encountered during the flight inspection of the davison GS, and going overhead lyh we failed to turn to the proper heading to join the arrival. I thought I had loaded and activated the STAR in our trimble GPS but apparently had not. ATC queried us as to whether we were on the arrival, and we made the proper course correction. No traffic conflicts were noted by ATC nor our TCASII equipment. One of the human factors involved was crew composition. I had a new hire pilot and a fairly inexperienced airborne technician. Our discussion during the en route portion of the flight was about an out of tolerance condition we found on the flight check of the GS.
Original NASA ASRS Text
Title: BE300 CREW DEVIATED FROM ARR RTE IN ZDC AIRSPACE.
Narrative: THE CREW WAS ENRTE TO GREENSBORO, NC, VIA LYH VORTAC AND THE HENBY STAR. WE WERE DISCUSSING THE PROBS WE ENCOUNTERED DURING THE FLT INSPECTION OF THE DAVISON GS, AND GOING OVERHEAD LYH WE FAILED TO TURN TO THE PROPER HEADING TO JOIN THE ARR. I THOUGHT I HAD LOADED AND ACTIVATED THE STAR IN OUR TRIMBLE GPS BUT APPARENTLY HAD NOT. ATC QUERIED US AS TO WHETHER WE WERE ON THE ARR, AND WE MADE THE PROPER COURSE CORRECTION. NO TFC CONFLICTS WERE NOTED BY ATC NOR OUR TCASII EQUIP. ONE OF THE HUMAN FACTORS INVOLVED WAS CREW COMPOSITION. I HAD A NEW HIRE PLT AND A FAIRLY INEXPERIENCED AIRBORNE TECHNICIAN. OUR DISCUSSION DURING THE ENRTE PORTION OF THE FLT WAS ABOUT AN OUT OF TOLERANCE CONDITION WE FOUND ON THE FLT CHK OF THE GS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.