37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 411421 |
Time | |
Date | 199808 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz |
State Reference | US |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : mht |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 411421 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Aircraft xyz air carrier returned because of a #2 engine bleed air problem. I performed (along with another technician) a pneumatic inspection and check of the #2 engine bleed system the night before the aircraft air returned. When I left work, the test of the #2 engine bleed system was working within limits of work card. Callback conversation with reporter revealed the following information: the reporter stated the aircraft had a #2 engine pneumatic report and troubleshooting revealed the precooler valve was the problem and the valve was replaced. The reporter said that sometime during the replacement of the precooler valve the pressure regulator shutoff valve lockout mechanism became engaged and locked the valve closed. The reporter stated no engine run was performed to test the engine pneumatic system after the precooler valve replacement. The reporter said the pressure regulator and shutoff valve locking mechanism lock bolt must have been loose and the valve locking block must have been bumped and pushed into the locking slot.
Original NASA ASRS Text
Title: A B737-300 WAS DISPATCHED AND RETURNED TO THE FIELD AFTER MAINT DUE TO #2 ENG PNEUMATIC SYS INOP DUE TO A VALVE INADVERTENTLY LOCKED CLOSED.
Narrative: ACFT XYZ ACR RETURNED BECAUSE OF A #2 ENG BLEED AIR PROB. I PERFORMED (ALONG WITH ANOTHER TECHNICIAN) A PNEUMATIC INSPECTION AND CHK OF THE #2 ENG BLEED SYS THE NIGHT BEFORE THE ACFT AIR RETURNED. WHEN I LEFT WORK, THE TEST OF THE #2 ENG BLEED SYS WAS WORKING WITHIN LIMITS OF WORK CARD. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ACFT HAD A #2 ENG PNEUMATIC RPT AND TROUBLESHOOTING REVEALED THE PRECOOLER VALVE WAS THE PROB AND THE VALVE WAS REPLACED. THE RPTR SAID THAT SOMETIME DURING THE REPLACEMENT OF THE PRECOOLER VALVE THE PRESSURE REGULATOR SHUTOFF VALVE LOCKOUT MECHANISM BECAME ENGAGED AND LOCKED THE VALVE CLOSED. THE RPTR STATED NO ENG RUN WAS PERFORMED TO TEST THE ENG PNEUMATIC SYS AFTER THE PRECOOLER VALVE REPLACEMENT. THE RPTR SAID THE PRESSURE REGULATOR AND SHUTOFF VALVE LOCKING MECHANISM LOCK BOLT MUST HAVE BEEN LOOSE AND THE VALVE LOCKING BLOCK MUST HAVE BEEN BUMPED AND PUSHED INTO THE LOCKING SLOT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.