Narrative:

Cockpit heard 4 chimes, therefore, aborted takeoff. None of the cabin crew rang the 4 chimes. It seems that there was an electrical short, as this had happened to one of the cockpit crew members a couple of days earlier. Tires were very hot and had to cool down, then developed a hydraulic leak. Airplane taken OTS. Supplemental information from acn 412109: this was due to 4 bell chime, our signal for an emergency in the cabin, in the cockpit. Indicator showed the evacuate/evacuation call came from 1L jump seat. This was impossible as I was seated in 1R jump seat and 1L flight attendant did not call the cockpit.

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Original NASA ASRS Text

Title: ON TKOF ON BOARD MD11, 4 CHIME EMER SIGNAL CAUSED FLC TO ABORT TKOF. ACFT RETURNED TO GATE WITHOUT INCIDENT AND WAS TAKEN OTS WITH HYD LEAK.

Narrative: COCKPIT HEARD 4 CHIMES, THEREFORE, ABORTED TKOF. NONE OF THE CABIN CREW RANG THE 4 CHIMES. IT SEEMS THAT THERE WAS AN ELECTRICAL SHORT, AS THIS HAD HAPPENED TO ONE OF THE COCKPIT CREW MEMBERS A COUPLE OF DAYS EARLIER. TIRES WERE VERY HOT AND HAD TO COOL DOWN, THEN DEVELOPED A HYD LEAK. AIRPLANE TAKEN OTS. SUPPLEMENTAL INFO FROM ACN 412109: THIS WAS DUE TO 4 BELL CHIME, OUR SIGNAL FOR AN EMER IN THE CABIN, IN THE COCKPIT. INDICATOR SHOWED THE EVAC CALL CAME FROM 1L JUMP SEAT. THIS WAS IMPOSSIBLE AS I WAS SEATED IN 1R JUMP SEAT AND 1L FLT ATTENDANT DID NOT CALL THE COCKPIT.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.