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|
Attributes | |
ACN | 413428 |
Time | |
Date | 199809 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : bos |
State Reference | MA |
Altitude | agl bound lower : 0 agl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : bos tracon : cvg |
Operator | common carrier : air carrier |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : initial climbout : takeoff ground other : taxi |
Route In Use | departure other departure sid : sid enroute other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : cfi |
Experience | flight time last 90 days : 170 flight time total : 6000 flight time type : 510 |
ASRS Report | 413428 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | non adherence : published procedure other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | controller : issued new clearance flight crew : returned to intended course or assigned course |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Bos clearance inquired if we could accept wylyy 1 departure instead of logan 2 as cleared on pre departure clearance. We consulted procedure. We verified that we were 'slant F.' discussed note about updating navigation system to runway 27 latitude/longitude prior to departure. This aircraft does not have takeoff shift feature. We agreed to do a quick alignment on runway and accepted departure. During taxi out, FMS caused a route discontinuity from the runway heading fix to garve waypoint. Repaired discontinuity 2 times. Took position on runway and did a quick IRS alignment. Flew departure in LNAV. After 1000 ft AGL, engaged autoplt. Aircraft immediately started a large right turn that appeared excessive. Downgraded autoplt to control wheel steering and re-engaged LNAV. Course bar began to swing back and forth 180 degrees every 10 seconds. Waypoint indicator appeared to be pointing to next fix, wylyy, but course information was erratic and unusable. Requested vectors from ATC. ATC queried reason for vectors. We advised them of unreliable navigation data. Rest of departure uneventful.
Original NASA ASRS Text
Title: B737 CREW DEVIATES FROM CLRED TRACK IN BOS AIRSPACE.
Narrative: BOS CLRNC INQUIRED IF WE COULD ACCEPT WYLYY 1 DEP INSTEAD OF LOGAN 2 AS CLRED ON PDC. WE CONSULTED PROC. WE VERIFIED THAT WE WERE 'SLANT F.' DISCUSSED NOTE ABOUT UPDATING NAV SYS TO RWY 27 LATITUDE/LONGITUDE PRIOR TO DEP. THIS ACFT DOES NOT HAVE TKOF SHIFT FEATURE. WE AGREED TO DO A QUICK ALIGNMENT ON RWY AND ACCEPTED DEP. DURING TAXI OUT, FMS CAUSED A RTE DISCONTINUITY FROM THE RWY HDG FIX TO GARVE WAYPOINT. REPAIRED DISCONTINUITY 2 TIMES. TOOK POS ON RWY AND DID A QUICK IRS ALIGNMENT. FLEW DEP IN LNAV. AFTER 1000 FT AGL, ENGAGED AUTOPLT. ACFT IMMEDIATELY STARTED A LARGE R TURN THAT APPEARED EXCESSIVE. DOWNGRADED AUTOPLT TO CTL WHEEL STEERING AND RE-ENGAGED LNAV. COURSE BAR BEGAN TO SWING BACK AND FORTH 180 DEGS EVERY 10 SECONDS. WAYPOINT INDICATOR APPEARED TO BE POINTING TO NEXT FIX, WYLYY, BUT COURSE INFO WAS ERRATIC AND UNUSABLE. REQUESTED VECTORS FROM ATC. ATC QUERIED REASON FOR VECTORS. WE ADVISED THEM OF UNRELIABLE NAV DATA. REST OF DEP UNEVENTFUL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.