37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 414291 |
Time | |
Date | 199809 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : prc |
State Reference | AZ |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zob |
Operator | general aviation : instructional |
Make Model Name | Duchess 76 |
Operating Under FAR Part | Part 91 |
Flight Phase | landing other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot instruction : instructor |
Qualification | pilot : instrument pilot : commercial pilot : cfi |
Experience | flight time last 90 days : 50 flight time total : 1700 flight time type : 170 |
ASRS Report | 414291 |
Person 2 | |
Affiliation | Other |
Function | flight crew : single pilot instruction : trainee |
Qualification | pilot : private |
Events | |
Anomaly | other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | other Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
A training flight. Practicing simulated single engine. Slight crosswind. Student put in appropriate crosswind correction. In flare, student rapidly reduced throttle and removed crosswind correction. It was gusting outside. Airspeed rapidly depleted outside sink rate envelope. Both instructor and student reacted to make appropriate corrections. Resulted in hard landing. After shutdown and inspection, instructor and student noticed propeller had been struck. (Although corrective actions were taken it was too late.)
Original NASA ASRS Text
Title: PROP STRIKE RESULTED TO A BE20 AFTER A HARD LNDG IN GUSTY XWINDS DURING MULTI ENG TRAINING. BOTH OF THE 2 ENG PROPS WERE DAMAGED.
Narrative: A TRAINING FLT. PRACTICING SIMULATED SINGLE ENG. SLIGHT XWIND. STUDENT PUT IN APPROPRIATE XWIND CORRECTION. IN FLARE, STUDENT RAPIDLY REDUCED THROTTLE AND REMOVED XWIND CORRECTION. IT WAS GUSTING OUTSIDE. AIRSPD RAPIDLY DEPLETED OUTSIDE SINK RATE ENVELOPE. BOTH INSTRUCTOR AND STUDENT REACTED TO MAKE APPROPRIATE CORRECTIONS. RESULTED IN HARD LNDG. AFTER SHUTDOWN AND INSPECTION, INSTRUCTOR AND STUDENT NOTICED PROP HAD BEEN STRUCK. (ALTHOUGH CORRECTIVE ACTIONS WERE TAKEN IT WAS TOO LATE.)
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.