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|
Attributes | |
ACN | 430734 |
Time | |
Date | 199903 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : sgf.airport |
State Reference | MO |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | SF 340A |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : taxi |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : commercial pilot : atp pilot : cfi pilot : multi engine |
Experience | flight time last 90 days : 100 flight time total : 8100 flight time type : 4000 |
ASRS Report | 430734 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : multi engine pilot : commercial |
Experience | flight time total : 2300 flight time type : 250 |
ASRS Report | 431073 |
Events | |
Anomaly | ground encounters other non adherence : company policies |
Independent Detector | other other : cgp 3 |
Resolutory Action | none taken : detected after the fact |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
The station agents at sgf had asked us to do a quick turn. While boarding, #2 engine was started. With the passenger on board and the paperwork and security check complete, I tried to get the ramper's attention to start #1 engine. They continued to have their conversation out at the left wingtip. While ignoring my signals for at least 5 mins, finally one of them cleared me. While the ramper moved from the left wingtip toward the nose, I signaled him to remove the chocks and continued with the after start flows and checks. Everything in the cockpit was completed in a normal and timely fashion. I then spent another five or more minutes trying to get the ramper to marshall us out. He stood about 75 ft in front of the nose, angled so his back was toward us. I flashed taxi and landing lights at him, but he continued to ignore us. By this time we had only enough fuel to taxi and meet our release fuel at takeoff after sitting for 15 minutes with the engines running. I used the mirrored wall of the terminal to insure no ground equipment was in the way and taxiied out. While taxiing toward the runway, the station called and said we had jumped the chocks, and the ramper had been ignoring us because we weren't supposed to leave for another 15 minutes. The pullout from the gate was normal in all aspects. Upon arrival in dfw I made a log entry. Maintenance inspected the nose gear with no discrepencies found. The station use of the term 'jump the chocks' was literal rather than actual. The ramper never turned toward us until after we left the gate. The chocks were not tight on the nose gear to begin with. I had been moving the tiller while flashing the taxi light, further loosening the chocks. So if he had not removed the chocks when signaled to, then we taxiied out the right side of them. In retrospect there was a total breakdown of communication at the station. The agents never informed the rampers of the quick turn. Next time I'll just shut everything down until the station gets it straightened out.
Original NASA ASRS Text
Title: CAPT OF A SAAB SF340 TAXIED OVER THE WHEEL CHOCKS LEAVING GATE PARKING SINCE THE RAMP GUIDANCE MARSHAL WAS NOT LOOKING OR RESPONDING TO THE FLC'S SIGNALS FOR LEAVING THE RAMP. MAINT PERSONNEL CHKED FOR ACFT DAMAGE UPON DEST ARR AND FOUND NONE.
Narrative: THE STATION AGENTS AT SGF HAD ASKED US TO DO A QUICK TURN. WHILE BOARDING, #2 ENG WAS STARTED. WITH THE PAX ON BOARD AND THE PAPERWORK AND SECURITY CHK COMPLETE, I TRIED TO GET THE RAMPER'S ATTN TO START #1 ENG. THEY CONTINUED TO HAVE THEIR CONVERSATION OUT AT THE L WINGTIP. WHILE IGNORING MY SIGNALS FOR AT LEAST 5 MINS, FINALLY ONE OF THEM CLRED ME. WHILE THE RAMPER MOVED FROM THE L WINGTIP TOWARD THE NOSE, I SIGNALED HIM TO REMOVE THE CHOCKS AND CONTINUED WITH THE AFTER START FLOWS AND CHKS. EVERYTHING IN THE COCKPIT WAS COMPLETED IN A NORMAL AND TIMELY FASHION. I THEN SPENT ANOTHER FIVE OR MORE MINUTES TRYING TO GET THE RAMPER TO MARSHALL US OUT. HE STOOD ABOUT 75 FT IN FRONT OF THE NOSE, ANGLED SO HIS BACK WAS TOWARD US. I FLASHED TAXI AND LNDG LIGHTS AT HIM, BUT HE CONTINUED TO IGNORE US. BY THIS TIME WE HAD ONLY ENOUGH FUEL TO TAXI AND MEET OUR RELEASE FUEL AT TKOF AFTER SITTING FOR 15 MINUTES WITH THE ENGINES RUNNING. I USED THE MIRRORED WALL OF THE TERMINAL TO INSURE NO GND EQUIP WAS IN THE WAY AND TAXIIED OUT. WHILE TAXIING TOWARD THE RWY, THE STATION CALLED AND SAID WE HAD JUMPED THE CHOCKS, AND THE RAMPER HAD BEEN IGNORING US BECAUSE WE WEREN'T SUPPOSED TO LEAVE FOR ANOTHER 15 MINUTES. THE PULLOUT FROM THE GATE WAS NORMAL IN ALL ASPECTS. UPON ARR IN DFW I MADE A LOG ENTRY. MAINT INSPECTED THE NOSE GEAR WITH NO DISCREPENCIES FOUND. THE STATION USE OF THE TERM 'JUMP THE CHOCKS' WAS LITERAL RATHER THAN ACTUAL. THE RAMPER NEVER TURNED TOWARD US UNTIL AFTER WE LEFT THE GATE. THE CHOCKS WERE NOT TIGHT ON THE NOSE GEAR TO BEGIN WITH. I HAD BEEN MOVING THE TILLER WHILE FLASHING THE TAXI LIGHT, FURTHER LOOSENING THE CHOCKS. SO IF HE HAD NOT REMOVED THE CHOCKS WHEN SIGNALED TO, THEN WE TAXIIED OUT THE R SIDE OF THEM. IN RETROSPECT THERE WAS A TOTAL BREAKDOWN OF COM AT THE STATION. THE AGENTS NEVER INFORMED THE RAMPERS OF THE QUICK TURN. NEXT TIME I'LL JUST SHUT EVERYTHING DOWN UNTIL THE STATION GETS IT STRAIGHTENED OUT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.