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|
Attributes | |
ACN | 434621 |
Time | |
Date | 199904 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : tpa.tracon |
State Reference | FL |
Altitude | msl bound lower : 1600 msl bound upper : 2600 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : tpa.tracon |
Operator | common carrier : air carrier |
Make Model Name | A320 |
Operating Under FAR Part | Part 121 |
Flight Phase | descent : approach |
Route In Use | approach : visual |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : flight engineer pilot : instrument pilot : multi engine |
Experience | flight time last 90 days : 172 flight time total : 2178 flight time type : 226 |
ASRS Report | 434621 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | other anomaly |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | aircraft : automation overrode flight crew controller : provided flight assist flight crew : overrode automation flight crew : regained aircraft control flight crew : executed go around |
Supplementary | |
Problem Areas | Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
On visual approach to runway 35R at pie, landing checklists completed, I called for the flight directors to be turned off. The captain did not hear and left his on. I turned off the autoplt and began descending manually. At approximately 800 ft, the FMA went to climb from speed and the motors began to spool to climb power. The captain and I realized something was wrong, but at the time didn't know what it was. The captain moved the thrust levers from the climb detent (normal position) to idle, causing the fadec to revert to idle. We had already flattened out the approach too much to land, so I called for a go around. During the go around, the autothrust had been turned off and the heading bug left at 090 degrees from when the autoplt was turning off. The instructions were to climb to 1600 ft and turn left to 270 degrees. Trying to level at 1600 ft, the speed was increasing rapidly, causing the plane to climb. At 2600 ft, we realized that the autothrust was off. I turned on the autothrust and autoplt at the same time. The aircraft stopped its acceleration and leveled at 2600 ft, but started turning toward 090 degrees to the right. I turned the heading bug to 270 degrees and the plane turned back to the left. Finally, everything was normal. We landed at pie with no further incident. Probable causes: lack of follow-up, CRM, lack of proper roles of PF/PNF. Solutions: better CRM and understanding roles of captain/first officer and PF/PNF.
Original NASA ASRS Text
Title: AN ACR FLC FLYING A320 AT PIE FAILS TO SET THE PROPER FLT DIRECTOR MODE FOR A VISUAL APCH WHICH RESULTS IN A GAR.
Narrative: ON VISUAL APCH TO RWY 35R AT PIE, LNDG CHKLISTS COMPLETED, I CALLED FOR THE FLT DIRECTORS TO BE TURNED OFF. THE CAPT DID NOT HEAR AND LEFT HIS ON. I TURNED OFF THE AUTOPLT AND BEGAN DSNDING MANUALLY. AT APPROX 800 FT, THE FMA WENT TO CLB FROM SPD AND THE MOTORS BEGAN TO SPOOL TO CLB PWR. THE CAPT AND I REALIZED SOMETHING WAS WRONG, BUT AT THE TIME DIDN'T KNOW WHAT IT WAS. THE CAPT MOVED THE THRUST LEVERS FROM THE CLB DETENT (NORMAL POS) TO IDLE, CAUSING THE FADEC TO REVERT TO IDLE. WE HAD ALREADY FLATTENED OUT THE APCH TOO MUCH TO LAND, SO I CALLED FOR A GAR. DURING THE GAR, THE AUTOTHRUST HAD BEEN TURNED OFF AND THE HDG BUG LEFT AT 090 DEGS FROM WHEN THE AUTOPLT WAS TURNING OFF. THE INSTRUCTIONS WERE TO CLB TO 1600 FT AND TURN L TO 270 DEGS. TRYING TO LEVEL AT 1600 FT, THE SPD WAS INCREASING RAPIDLY, CAUSING THE PLANE TO CLB. AT 2600 FT, WE REALIZED THAT THE AUTOTHRUST WAS OFF. I TURNED ON THE AUTOTHRUST AND AUTOPLT AT THE SAME TIME. THE ACFT STOPPED ITS ACCELERATION AND LEVELED AT 2600 FT, BUT STARTED TURNING TOWARD 090 DEGS TO THE R. I TURNED THE HDG BUG TO 270 DEGS AND THE PLANE TURNED BACK TO THE L. FINALLY, EVERYTHING WAS NORMAL. WE LANDED AT PIE WITH NO FURTHER INCIDENT. PROBABLE CAUSES: LACK OF FOLLOW-UP, CRM, LACK OF PROPER ROLES OF PF/PNF. SOLUTIONS: BETTER CRM AND UNDERSTANDING ROLES OF CAPT/FO AND PF/PNF.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.