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|
Attributes | |
ACN | 437932 |
Time | |
Date | 199905 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | navaid : har.vortac |
State Reference | PA |
Altitude | msl single value : 18000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | artcc : zny.artcc |
Operator | common carrier : air carrier |
Make Model Name | DC-8 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | other vortac |
Flight Phase | climbout : vacating altitude |
Route In Use | enroute : direct |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 110 flight time total : 15800 flight time type : 2500 |
ASRS Report | 437932 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : multi engine pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : oil quantity other flight crewa other flight crewb |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance Maintenance Human Performance |
Primary Problem | Aircraft |
Narrative:
Noticed #4 oil pressure low light flicker. Asked the flight engineer what the pressure gauge was doing. Pressure gauge showing fluctuations and oil quantity had decreased to 1-2 gallons. We secured #4 engine. We had departed jfk en route to iln. WX, fuel, and performance permitted us to safely continue to iln. After landing, there was no indication of where the oil quantity had gone, but reservoir was empty.
Original NASA ASRS Text
Title: DC8-61 FLC SHUTS DOWN ENG INFLT DUE TO LOW OIL QUANTITY.
Narrative: NOTICED #4 OIL PRESSURE LOW LIGHT FLICKER. ASKED THE FE WHAT THE PRESSURE GAUGE WAS DOING. PRESSURE GAUGE SHOWING FLUCTUATIONS AND OIL QUANTITY HAD DECREASED TO 1-2 GALLONS. WE SECURED #4 ENG. WE HAD DEPARTED JFK ENRTE TO ILN. WX, FUEL, AND PERFORMANCE PERMITTED US TO SAFELY CONTINUE TO ILN. AFTER LNDG, THERE WAS NO INDICATION OF WHERE THE OIL QUANTITY HAD GONE, BUT RESERVOIR WAS EMPTY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.