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|
Attributes | |
ACN | 468641 |
Time | |
Date | 200004 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : anc.airport |
State Reference | AK |
Altitude | msl single value : 5000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : a11.tracon |
Operator | common carrier : air carrier |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : initial |
Route In Use | departure sid : n/s |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 100 flight time total : 15000 flight time type : 2000 |
ASRS Report | 468641 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : multi engine pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft |
Primary Problem | Flight Crew Human Performance |
Narrative:
Shortly after takeoff, autopressurization failed. Ran checklist and determined that cabin could not be pressurized in automatic, standby, or manual. Notified flight attendants of possible return. Flight attendant called back and told us that there was a noticeable air noise at the bottom of door L2. With indications of a door seal problem we returned to the airport. Shortly after we got back on the ground, I got this nagging feeling that we had taken off unpressurized. Maintenance investigation showed the door to be ok. After initial pushback we had the aircraft deiced. Deicing calls for the engine bleeds to be turned off and remain off for 1 min after deicing to help prevent fluid from entering the ducts. I want to believe that we turned the bleeds back on because we went so far as to start the clock for a 1 min timing, and both noted when 1 min was up. Maintenance changed the pressure controller as a precaution, and we were eventually on our way. This event again shows the need to be extra vigilant whenever deviating from the routine.
Original NASA ASRS Text
Title: B737 DOES NOT PRESSURIZE AFTER TKOF FROM ANC, AK.
Narrative: SHORTLY AFTER TKOF, AUTOPRESSURIZATION FAILED. RAN CHKLIST AND DETERMINED THAT CABIN COULD NOT BE PRESSURIZED IN AUTO, STANDBY, OR MANUAL. NOTIFIED FLT ATTENDANTS OF POSSIBLE RETURN. FLT ATTENDANT CALLED BACK AND TOLD US THAT THERE WAS A NOTICEABLE AIR NOISE AT THE BOTTOM OF DOOR L2. WITH INDICATIONS OF A DOOR SEAL PROB WE RETURNED TO THE ARPT. SHORTLY AFTER WE GOT BACK ON THE GND, I GOT THIS NAGGING FEELING THAT WE HAD TAKEN OFF UNPRESSURIZED. MAINT INVESTIGATION SHOWED THE DOOR TO BE OK. AFTER INITIAL PUSHBACK WE HAD THE ACFT DEICED. DEICING CALLS FOR THE ENG BLEEDS TO BE TURNED OFF AND REMAIN OFF FOR 1 MIN AFTER DEICING TO HELP PREVENT FLUID FROM ENTERING THE DUCTS. I WANT TO BELIEVE THAT WE TURNED THE BLEEDS BACK ON BECAUSE WE WENT SO FAR AS TO START THE CLOCK FOR A 1 MIN TIMING, AND BOTH NOTED WHEN 1 MIN WAS UP. MAINT CHANGED THE PRESSURE CTLR AS A PRECAUTION, AND WE WERE EVENTUALLY ON OUR WAY. THIS EVENT AGAIN SHOWS THE NEED TO BE EXTRA VIGILANT WHENEVER DEVIATING FROM THE ROUTINE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.