37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 474581 |
Time | |
Date | 200005 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : sdf.airport |
State Reference | KY |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : sdf.tower |
Operator | common carrier : air carrier |
Make Model Name | DC-8 70 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : initial |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : multi engine pilot : commercial pilot : atp pilot : instrument pilot : flight engineer |
Experience | flight time last 90 days : 40 flight time total : 4700 flight time type : 600 |
ASRS Report | 474581 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe non adherence : published procedure non adherence : company policies other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Company |
Primary Problem | Flight Crew Human Performance |
Narrative:
After takeoff on a hot standby assignment the main gear would not properly retract. After following the appropriate checklists, talking to flight control, and maintenance, the decision was made to return to sdf. All hydraulic system with the exception of the gear operated normally. Abnormal hydraulic indications were noted and system pressure was normal. The landing was uneventful. After the aircraft was secured we debrief with maintenance in the cockpit. A day later I was informed that the hydraulic system selector was found out of the normal detent. I did my normal preflight which includes checking the hydraulic system selector. The hydraulic system selector was left in the normal position. Again, during the flight all hydraulic system with exception of the main gear operated normally.
Original NASA ASRS Text
Title: DC8 CREW WAS UNABLE TO RETRACT THE LNDG GEAR AFTER TKOF.
Narrative: AFTER TKOF ON A HOT STANDBY ASSIGNMENT THE MAIN GEAR WOULD NOT PROPERLY RETRACT. AFTER FOLLOWING THE APPROPRIATE CHKLISTS, TALKING TO FLT CTL, AND MAINT, THE DECISION WAS MADE TO RETURN TO SDF. ALL HYD SYS WITH THE EXCEPTION OF THE GEAR OPERATED NORMALLY. ABNORMAL HYD INDICATIONS WERE NOTED AND SYS PRESSURE WAS NORMAL. THE LNDG WAS UNEVENTFUL. AFTER THE ACFT WAS SECURED WE DEBRIEF WITH MAINT IN THE COCKPIT. A DAY LATER I WAS INFORMED THAT THE HYD SYS SELECTOR WAS FOUND OUT OF THE NORMAL DETENT. I DID MY NORMAL PREFLT WHICH INCLUDES CHKING THE HYD SYS SELECTOR. THE HYD SYS SELECTOR WAS LEFT IN THE NORMAL POS. AGAIN, DURING THE FLT ALL HYD SYS WITH EXCEPTION OF THE MAIN GEAR OPERATED NORMALLY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.