Narrative:

All preflight, taxi and takeoff checks were accomplished and normal. We were on a STAR and had commenced climbing. Suddenly, we heard a loud air rushing sound. Almost simultaneously, the cabin interphone rang. While picking up the phone, I checked the pressurization and airflow. Both were normal. At about this point we got an EICAS message and an overhead discrete light both announcing a problem with the right forward door. The interphone call was from a flight attendant confirming our cockpit indications. The next few mins were very busy with checklists, communications and procedures. An uneventful landing was made, repairs were effected, an overweight landing inspection was made and we were back underway within 1 hour.

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Original NASA ASRS Text

Title: A B757-200 ON INITIAL CLB AT 5000 FT DIVERTED DUE TO #1 R DOOR NOT CLOSED AND LOCKED DUE TO FALSE LATCHING.

Narrative: ALL PREFLT, TAXI AND TKOF CHKS WERE ACCOMPLISHED AND NORMAL. WE WERE ON A STAR AND HAD COMMENCED CLBING. SUDDENLY, WE HEARD A LOUD AIR RUSHING SOUND. ALMOST SIMULTANEOUSLY, THE CABIN INTERPHONE RANG. WHILE PICKING UP THE PHONE, I CHKED THE PRESSURIZATION AND AIRFLOW. BOTH WERE NORMAL. AT ABOUT THIS POINT WE GOT AN EICAS MESSAGE AND AN OVERHEAD DISCRETE LIGHT BOTH ANNOUNCING A PROB WITH THE R FORWARD DOOR. THE INTERPHONE CALL WAS FROM A FLT ATTENDANT CONFIRMING OUR COCKPIT INDICATIONS. THE NEXT FEW MINS WERE VERY BUSY WITH CHKLISTS, COMS AND PROCS. AN UNEVENTFUL LNDG WAS MADE, REPAIRS WERE EFFECTED, AN OVERWT LNDG INSPECTION WAS MADE AND WE WERE BACK UNDERWAY WITHIN 1 HR.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.