37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 475609 |
Time | |
Date | 200006 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : lax.airport |
State Reference | CA |
Altitude | agl single value : 50 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : lax.tower |
Operator | common carrier : air carrier |
Make Model Name | B727-100 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : initial |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : multi engine pilot : instrument pilot : flight engineer pilot : cfi pilot : commercial |
Experience | flight time last 90 days : 180 flight time total : 3200 flight time type : 2100 |
ASRS Report | 475609 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | other anomaly other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
During takeoff from lax the crew smelled burning rubber in the cockpit. We put on our oxygen masks, declared an emergency and returned to the field. The landing was uneventful and there was no indication we had a fire. The mechanics think it was something in the pressurization system. I think that we did everything correctly. After getting a new airplane we continued our day which lasted a total of 14 hours. At the time I thought I was rested enough for the following trips, but looking back I think the emergency really drained me and I should have had some rest before flying a long day.
Original NASA ASRS Text
Title: B727 IN CARGO OP HAD SMELL IN COCKPIT AFTER TKOF. RETURNED TO LAND. AIR CONDITIONING PROB WAS FOUND. RPTR CONCERNED ABOUT EFFECT STRESS HAD ON REMAINDER OF DUTY DAY.
Narrative: DURING TKOF FROM LAX THE CREW SMELLED BURNING RUBBER IN THE COCKPIT. WE PUT ON OUR OXYGEN MASKS, DECLARED AN EMER AND RETURNED TO THE FIELD. THE LNDG WAS UNEVENTFUL AND THERE WAS NO INDICATION WE HAD A FIRE. THE MECHS THINK IT WAS SOMETHING IN THE PRESSURIZATION SYS. I THINK THAT WE DID EVERYTHING CORRECTLY. AFTER GETTING A NEW AIRPLANE WE CONTINUED OUR DAY WHICH LASTED A TOTAL OF 14 HRS. AT THE TIME I THOUGHT I WAS RESTED ENOUGH FOR THE FOLLOWING TRIPS, BUT LOOKING BACK I THINK THE EMER REALLY DRAINED ME AND I SHOULD HAVE HAD SOME REST BEFORE FLYING A LONG DAY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.