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|
Attributes | |
ACN | 483560 |
Time | |
Date | 200008 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : anc.airport |
State Reference | AK |
Altitude | agl single value : 0 |
Aircraft 1 | |
Controlling Facilities | tower : anc.tower |
Operator | common carrier : air carrier |
Make Model Name | B737-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : parked |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 230 flight time total : 12000 flight time type : 9000 |
ASRS Report | 483560 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 240 flight time total : 17000 flight time type : 9000 |
ASRS Report | 484057 |
Events | |
Anomaly | aircraft equipment problem : less severe maintenance problem : improper documentation non adherence : published procedure non adherence : company policies non adherence : far other anomaly other |
Independent Detector | other other : pers 5 |
Resolutory Action | none taken : detected after the fact |
Consequence | faa : reviewed incident with flight crew |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft Company Maintenance Human Performance FAA |
Primary Problem | Flight Crew Human Performance |
Narrative:
Nearing departure time on a nearly full flight to otz-ome, FAA jump seater set up primary jump seat, only to discover the 5TH (crotch) strap/belt was missing. Consultations with local maintenance and maintenance control resulted in issuing an MEL for the belt, allowing the seat to still be used. All maintenance related paperwork (discrepancy entered in maintenance logbook, aircraft released to fly by maintenance, MEL placarding, etc), done in correct manner. Departed gate xx mins late due to this matter. Taxied and took off normally. When passing 'off' time to company operations, agent read us the revision to our dispatch release, which we should have received before takeoff. I attribute this procedural breakdown to: 1) hurry-up-itis. We were late and getting later on a trip that has 3 stops and short station times, with little chance to get back on schedule. 2) stress of having an FAA inspector giving us a line check. It is perhaps ironic that this inadvertent lapse was due in part to a problem with the very seat the inspector was occupying.
Original NASA ASRS Text
Title: WITH FAA ACR INSPECTOR ON BOARD, ACR CREW DEPARTS WITHOUT PROPER DISPATCH RELEASE.
Narrative: NEARING DEP TIME ON A NEARLY FULL FLT TO OTZ-OME, FAA JUMP SEATER SET UP PRIMARY JUMP SEAT, ONLY TO DISCOVER THE 5TH (CROTCH) STRAP/BELT WAS MISSING. CONSULTATIONS WITH LCL MAINT AND MAINT CTL RESULTED IN ISSUING AN MEL FOR THE BELT, ALLOWING THE SEAT TO STILL BE USED. ALL MAINT RELATED PAPERWORK (DISCREPANCY ENTERED IN MAINT LOGBOOK, ACFT RELEASED TO FLY BY MAINT, MEL PLACARDING, ETC), DONE IN CORRECT MANNER. DEPARTED GATE XX MINS LATE DUE TO THIS MATTER. TAXIED AND TOOK OFF NORMALLY. WHEN PASSING 'OFF' TIME TO COMPANY OPS, AGENT READ US THE REVISION TO OUR DISPATCH RELEASE, WHICH WE SHOULD HAVE RECEIVED BEFORE TKOF. I ATTRIBUTE THIS PROCEDURAL BREAKDOWN TO: 1) HURRY-UP-ITIS. WE WERE LATE AND GETTING LATER ON A TRIP THAT HAS 3 STOPS AND SHORT STATION TIMES, WITH LITTLE CHANCE TO GET BACK ON SCHEDULE. 2) STRESS OF HAVING AN FAA INSPECTOR GIVING US A LINE CHK. IT IS PERHAPS IRONIC THAT THIS INADVERTENT LAPSE WAS DUE IN PART TO A PROB WITH THE VERY SEAT THE INSPECTOR WAS OCCUPYING.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.