37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 487842 |
Time | |
Date | 200010 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ind.airport |
State Reference | IN |
Altitude | msl single value : 35000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zid.artcc tower : lax.tower |
Operator | common carrier : air carrier |
Make Model Name | Fokker 100 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | cruise : level |
Route In Use | enroute airway : j152.airway |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : multi engine pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 200 flight time total : 10500 flight time type : 750 |
ASRS Report | 487842 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : #2 engine indications other flight crewa other flight crewb |
Resolutory Action | controller : issued new clearance flight crew : declared emergency flight crew : diverted to another airport |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Cruise flight at FL350 and .72 mach, #2 engine failed. As power was reduced to slow for some chop conditions (light chop), #2 engine just spooled down and windmilled. An emergency was declared, we 'spiraled' down and landed at ind (diverted). Callback conversation with reporter revealed the following information: the reporter stated the engine was a rolls royce tay 650 and when entering light chop the throttles were retarded almost to idle the #2 engine spooled down. The reporter said on descent at 10000 ft a relight attempt was made with no success. The reporter said on the ground maintenance started the engine but ran it at idle only. The reporter said he was not advised by maintenance of the component that failed but suspects the engine driven fuel pump.
Original NASA ASRS Text
Title: A FOKKER IN CRUISE AT FL350 DECLARED AN EMER AND DIVERTED DUE TO #2 ENG SPOOLDOWN WITH NO RELIGHT.
Narrative: CRUISE FLT AT FL350 AND .72 MACH, #2 ENG FAILED. AS PWR WAS REDUCED TO SLOW FOR SOME CHOP CONDITIONS (LIGHT CHOP), #2 ENG JUST SPOOLED DOWN AND WINDMILLED. AN EMER WAS DECLARED, WE 'SPIRALED' DOWN AND LANDED AT IND (DIVERTED). CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ENG WAS A ROLLS ROYCE TAY 650 AND WHEN ENTERING LIGHT CHOP THE THROTTLES WERE RETARDED ALMOST TO IDLE THE #2 ENG SPOOLED DOWN. THE RPTR SAID ON DSCNT AT 10000 FT A RELIGHT ATTEMPT WAS MADE WITH NO SUCCESS. THE RPTR SAID ON THE GND MAINT STARTED THE ENG BUT RAN IT AT IDLE ONLY. THE RPTR SAID HE WAS NOT ADVISED BY MAINT OF THE COMPONENT THAT FAILED BUT SUSPECTS THE ENG DRIVEN FUEL PUMP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.