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|
Attributes | |
ACN | 503289 |
Time | |
Date | 200102 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : hnl.airport |
State Reference | HI |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B767 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | landing : roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time total : 13000 flight time type : 818 |
ASRS Report | 503289 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : multi engine pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft Maintenance Human Performance |
Narrative:
I was captain/PNF. Our approach was normal and we configured early. Normal callouts were made. I made 2 extra callouts of 'on speed sink 700 down' touchdown was in the touchdown zone. Touchdown was normal as the mains touched. Then as the nose gear was coming down, it pitched up abnormally. The nose gear had not touched down yet. Both my first officer and I pushed forward on the yoke to arrest the pitch-up. The pitch was not excessive, but it was abnormal. There was no danger to the airplane as we both quickly corrected the pitch. The remainder of the flight was uneventful. I believe the problem was with the ground spoilers. There was no bounce or skip. Callback conversation with reporter revealed the following information: the aircraft was returned to the maintenance base where it was determined that a safety wire had not been installed during a maintenance visit allowing linkage to depart the aircraft. The ground spoilers, as a result, only extended partially until engine thrust was reversed commanding full extension and the unexpected pitch up.
Original NASA ASRS Text
Title: B767 PITCH UP ON TOUCHDOWN AS A RESULT OF GND SPOILER PROB.
Narrative: I WAS CAPT/PNF. OUR APCH WAS NORMAL AND WE CONFIGURED EARLY. NORMAL CALLOUTS WERE MADE. I MADE 2 EXTRA CALLOUTS OF 'ON SPD SINK 700 DOWN' TOUCHDOWN WAS IN THE TOUCHDOWN ZONE. TOUCHDOWN WAS NORMAL AS THE MAINS TOUCHED. THEN AS THE NOSE GEAR WAS COMING DOWN, IT PITCHED UP ABNORMALLY. THE NOSE GEAR HAD NOT TOUCHED DOWN YET. BOTH MY FO AND I PUSHED FORWARD ON THE YOKE TO ARREST THE PITCH-UP. THE PITCH WAS NOT EXCESSIVE, BUT IT WAS ABNORMAL. THERE WAS NO DANGER TO THE AIRPLANE AS WE BOTH QUICKLY CORRECTED THE PITCH. THE REMAINDER OF THE FLT WAS UNEVENTFUL. I BELIEVE THE PROB WAS WITH THE GND SPOILERS. THERE WAS NO BOUNCE OR SKIP. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE ACFT WAS RETURNED TO THE MAINT BASE WHERE IT WAS DETERMINED THAT A SAFETY WIRE HAD NOT BEEN INSTALLED DURING A MAINT VISIT ALLOWING LINKAGE TO DEPART THE ACFT. THE GND SPOILERS, AS A RESULT, ONLY EXTENDED PARTIALLY UNTIL ENG THRUST WAS REVERSED COMMANDING FULL EXTENSION AND THE UNEXPECTED PITCH UP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.