Narrative:

During climb to FL230, we began having a problem trimming the aircraft nose-down. The nose-down electric trim would not work. The aircraft's electric trim began trimming nose-up, the autoplt was off. The captain was flying and was having a hard time landing nose-down. We decided to return to sfo. We were at FL230 when ATC cleared us to FL200 with a turn back to the airport. The captain began the descent and I started the QRH. I reminded him of our altitude. We were cleared to and turned around to look for popped circuit breakers. When I turned back around, he had descended to FL180. Once we slowed the airplane down, the trim began to work normally. I think the aircraft was loaded too far aft of center of gravity, but all of our paperwork indicated we were ok.

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Original NASA ASRS Text

Title: UPON RETURN TO ARPT FOR PRECAUTIONARY LNDG DUE TO MACH TRIM PROB, B737-200 FLC OVERSHOOT ASSIGNED ALT.

Narrative: DURING CLB TO FL230, WE BEGAN HAVING A PROB TRIMMING THE ACFT NOSE-DOWN. THE NOSE-DOWN ELECTRIC TRIM WOULD NOT WORK. THE ACFT'S ELECTRIC TRIM BEGAN TRIMMING NOSE-UP, THE AUTOPLT WAS OFF. THE CAPT WAS FLYING AND WAS HAVING A HARD TIME LNDG NOSE-DOWN. WE DECIDED TO RETURN TO SFO. WE WERE AT FL230 WHEN ATC CLRED US TO FL200 WITH A TURN BACK TO THE ARPT. THE CAPT BEGAN THE DSCNT AND I STARTED THE QRH. I REMINDED HIM OF OUR ALT. WE WERE CLRED TO AND TURNED AROUND TO LOOK FOR POPPED CIRCUIT BREAKERS. WHEN I TURNED BACK AROUND, HE HAD DSNDED TO FL180. ONCE WE SLOWED THE AIRPLANE DOWN, THE TRIM BEGAN TO WORK NORMALLY. I THINK THE ACFT WAS LOADED TOO FAR AFT OF CTR OF GRAVITY, BUT ALL OF OUR PAPERWORK INDICATED WE WERE OK.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.