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|
Attributes | |
ACN | 516514 |
Time | |
Date | 200107 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : lax.airport |
State Reference | CA |
Environment | |
Weather Elements | other |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : sct.tracon tower : msp.tower |
Operator | common carrier : air carrier |
Make Model Name | B767-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : initial |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight attendant : on duty |
Qualification | flight attendant : currently qualified flight attendant aircraft qualified on : 6 |
Experience | flight attendant time airline total : 28 flight attendant time total : 28 flight attendant time type : 90 |
ASRS Report | 516514 |
Person 2 | |
Affiliation | company : air carrier |
Function | oversight : flight attendant in charge |
Qualification | flight attendant : currently qualified |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : 1 |
Resolutory Action | flight crew : diverted to another airport none taken : detected after the fact other |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
I was sitting in my jump seat adjacent to the mid galley approximately 10 mins after takeoff. We had just completed the 180 degree turn out over the pacific and were heading back eastbound. All of a sudden, I noticed that the mid galley power went out as well as all the reading lights in the coach cabin. The cockpit told the purser we were turning around and going back to lax because we had lost a generator. Because of the significant decrease in airflow, I was having difficulty breathing, but as soon as I quit moving about the aircraft, I felt significantly better. Upon descent, the flight attendant across from me felt extraordinarily noticeable vibrations under her feet. Upon investigation, mechanics found a crack in the covering of the #1, l-hand engine.
Original NASA ASRS Text
Title: B767-200 CREW RETURNED TO LAX AFTER LOSS OF AN ACFT GENERATOR.
Narrative: I WAS SITTING IN MY JUMP SEAT ADJACENT TO THE MID GALLEY APPROX 10 MINS AFTER TKOF. WE HAD JUST COMPLETED THE 180 DEG TURN OUT OVER THE PACIFIC AND WERE HDG BACK EBOUND. ALL OF A SUDDEN, I NOTICED THAT THE MID GALLEY PWR WENT OUT AS WELL AS ALL THE READING LIGHTS IN THE COACH CABIN. THE COCKPIT TOLD THE PURSER WE WERE TURNING AROUND AND GOING BACK TO LAX BECAUSE WE HAD LOST A GENERATOR. BECAUSE OF THE SIGNIFICANT DECREASE IN AIRFLOW, I WAS HAVING DIFFICULTY BREATHING, BUT AS SOON AS I QUIT MOVING ABOUT THE ACFT, I FELT SIGNIFICANTLY BETTER. UPON DSCNT, THE FLT ATTENDANT ACROSS FROM ME FELT EXTRAORDINARILY NOTICEABLE VIBRATIONS UNDER HER FEET. UPON INVESTIGATION, MECHS FOUND A CRACK IN THE COVERING OF THE #1, L-HAND ENG.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.