37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 517814 |
Time | |
Date | 200107 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : t74.airport |
State Reference | TX |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Bonanza 36 |
Operating Under FAR Part | Part 91 |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : private |
Experience | flight time last 90 days : 5 flight time total : 500 flight time type : 200 |
ASRS Report | 517814 |
Events | |
Anomaly | ground encounters : gear up landing non adherence : published procedure non adherence : far other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | other other |
Supplementary | |
Problem Areas | Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
On the morning of jul/xa/01 at XA00 after landing at taylor field, on rollout, the gear retracted. I believe the cause was my right hand unintentionally hitting the gear lever while checking the RPM (propeller) control to be sure it was full forward.
Original NASA ASRS Text
Title: BE36 PLT CAUSED THE LNDG GEAR TO RETRACT DURING LNDG ROLLOUT.
Narrative: ON THE MORNING OF JUL/XA/01 AT XA00 AFTER LNDG AT TAYLOR FIELD, ON ROLLOUT, THE GEAR RETRACTED. I BELIEVE THE CAUSE WAS MY R HAND UNINTENTIONALLY HITTING THE GEAR LEVER WHILE CHKING THE RPM (PROP) CTL TO BE SURE IT WAS FULL FORWARD.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.