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|
Attributes | |
ACN | 518919 |
Time | |
Date | 200107 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : dfw.tower |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight attendant : on duty |
Qualification | flight attendant : currently qualified flight attendant aircraft qualified on : 8 |
Experience | flight attendant time airline total : 3 flight attendant time total : 3 flight attendant time type : 30 |
ASRS Report | 518919 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other anomaly other |
Independent Detector | other flight crewa other flight crewb other other : 1 (cab) |
Resolutory Action | flight crew : landed as precaution |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
As we climbed out of dfw, captain called back to see if there were 'hot smells' in aft portion of plane. We informed him it smelled like ovens were on (they were not on) and he informed us they were getting an air duct leak that made engine's temperature rise when engines were running on full power. We returned to dfw and airplane was removed from service. FYI, the plane had just returned to service after 1 1/2 days in maintenance facility trying to fix problem. Captain was great at including cabin crew in situation, used us as his eyes and ears, to help identify problem.
Original NASA ASRS Text
Title: SUPER MD80 FLC RETURN LAND AFTER HOT FUMES WERE SMELLED IN THE COCKPIT AND CABIN.
Narrative: AS WE CLBED OUT OF DFW, CAPT CALLED BACK TO SEE IF THERE WERE 'HOT SMELLS' IN AFT PORTION OF PLANE. WE INFORMED HIM IT SMELLED LIKE OVENS WERE ON (THEY WERE NOT ON) AND HE INFORMED US THEY WERE GETTING AN AIR DUCT LEAK THAT MADE ENG'S TEMP RISE WHEN ENGS WERE RUNNING ON FULL PWR. WE RETURNED TO DFW AND AIRPLANE WAS REMOVED FROM SVC. FYI, THE PLANE HAD JUST RETURNED TO SVC AFTER 1 1/2 DAYS IN MAINT FACILITY TRYING TO FIX PROB. CAPT WAS GREAT AT INCLUDING CABIN CREW IN SIT, USED US AS HIS EYES AND EARS, TO HELP IDENT PROB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.