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|
Attributes | |
ACN | 520851 |
Time | |
Date | 200102 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ofp.airport |
State Reference | VA |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : tpa.tower |
Operator | general aviation : corporate |
Make Model Name | Chancellor 414A & C414 |
Operating Under FAR Part | Part 91 |
Flight Phase | ground : taxi |
Flight Plan | None |
Person 1 | |
Affiliation | company : corporate |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | controller supervisory : 7 flight time last 90 days : 100 flight time total : 3620 flight time type : 300 |
ASRS Report | 520851 |
Person 2 | |
Affiliation | company : corporate |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical excursion : taxiway other anomaly other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : rt brake affectiveness other flight crewa |
Consequence | faa : investigated other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
On the morning of feb/xa/01, myself and 5 others taxied for departure from ofp to lns. At the end of the taxiway, I pwred the left engine to approximately 2000 RPM to pivot the C414 90 degrees to the runway. At that point I discovered the right brake had failed after I tested them when we left the chocks. I kept the power up to try to complete the turn, but it would not. This momentum carried the plane approximately 20 ft into a ditch, collapsing the nose gear. There were no injuries noted by anyone. It appears that a seal on the master cylinder failed behind the pilot's rudder pedals. Fluid was found inside the fuselage after the incident. There was no fluid present on the ground where the plane had been parked overnight. I perceived that using the one good brake would have carried the C414 off the left side of the taxiway and into a concrete culvert which is why I elected to shut down and taxi off the taxiway into a grassy field. The method that had been used to cut the field shadowed the ditch from my view or I would have taken different actions.
Original NASA ASRS Text
Title: CESSNA 414 PLT LOST CTL OF THE ACFT WHEN PWRING UP THE L ENG TO PIVOT TOWARD THE RWY.
Narrative: ON THE MORNING OF FEB/XA/01, MYSELF AND 5 OTHERS TAXIED FOR DEP FROM OFP TO LNS. AT THE END OF THE TXWY, I PWRED THE L ENG TO APPROX 2000 RPM TO PIVOT THE C414 90 DEGS TO THE RWY. AT THAT POINT I DISCOVERED THE R BRAKE HAD FAILED AFTER I TESTED THEM WHEN WE LEFT THE CHOCKS. I KEPT THE PWR UP TO TRY TO COMPLETE THE TURN, BUT IT WOULD NOT. THIS MOMENTUM CARRIED THE PLANE APPROX 20 FT INTO A DITCH, COLLAPSING THE NOSE GEAR. THERE WERE NO INJURIES NOTED BY ANYONE. IT APPEARS THAT A SEAL ON THE MASTER CYLINDER FAILED BEHIND THE PLT'S RUDDER PEDALS. FLUID WAS FOUND INSIDE THE FUSELAGE AFTER THE INCIDENT. THERE WAS NO FLUID PRESENT ON THE GND WHERE THE PLANE HAD BEEN PARKED OVERNIGHT. I PERCEIVED THAT USING THE ONE GOOD BRAKE WOULD HAVE CARRIED THE C414 OFF THE L SIDE OF THE TXWY AND INTO A CONCRETE CULVERT WHICH IS WHY I ELECTED TO SHUT DOWN AND TAXI OFF THE TXWY INTO A GRASSY FIELD. THE METHOD THAT HAD BEEN USED TO CUT THE FIELD SHADOWED THE DITCH FROM MY VIEW OR I WOULD HAVE TAKEN DIFFERENT ACTIONS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.