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|
Attributes | |
ACN | 545469 |
Time | |
Date | 200204 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : crg.airport |
State Reference | FL |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Operator | general aviation : instructional |
Make Model Name | Duchess 76 |
Operating Under FAR Part | Part 91 |
Flight Phase | climbout : takeoff |
Flight Plan | VFR |
Person 1 | |
Affiliation | other |
Function | instruction : instructor |
Qualification | pilot : multi engine pilot : cfi pilot : commercial |
Experience | flight time last 90 days : 225 flight time total : 700 flight time type : 35 |
ASRS Report | 545469 |
Person 2 | |
Affiliation | other |
Function | instruction : trainee |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | none taken : detected after the fact none taken : insufficient time |
Consequence | faa : investigated faa : reviewed incident with flight crew other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Performed a full stop landing and taxi back for departure at craig field, fl. Had 3 green lights on takeoff check. At approximately 45-50 KTS on takeoff roll, nose gear collapsed and aircraft skidded to stop damaging both propellers and nose cone. Originally it was assumed that landing gear handle was inadvertently placed in the 'up' position, and gear began retraction during the takeoff roll. Gear handle was found in 'down' position the following day, with no one being able to explain how it got in the down position. Further investigation, which included a gear swing, found excessive wear in the nose gear, causing the gear to easily move past the over-center, making it possible that a bump may have folded the gear forward. FAA investigation concluded that mechanical defect was the cause of this incident.
Original NASA ASRS Text
Title: BEECH 76 NOSE GEAR COLLAPSED ON TKOF ROLL CAUSING ACFT TO DROP ON RWY DAMAGING BOTH PROPS AND NOSE CONE.
Narrative: PERFORMED A FULL STOP LNDG AND TAXI BACK FOR DEP AT CRAIG FIELD, FL. HAD 3 GREEN LIGHTS ON TKOF CHK. AT APPROX 45-50 KTS ON TKOF ROLL, NOSE GEAR COLLAPSED AND ACFT SKIDDED TO STOP DAMAGING BOTH PROPS AND NOSE CONE. ORIGINALLY IT WAS ASSUMED THAT LNDG GEAR HANDLE WAS INADVERTENTLY PLACED IN THE 'UP' POS, AND GEAR BEGAN RETRACTION DURING THE TKOF ROLL. GEAR HANDLE WAS FOUND IN 'DOWN' POS THE FOLLOWING DAY, WITH NO ONE BEING ABLE TO EXPLAIN HOW IT GOT IN THE DOWN POS. FURTHER INVESTIGATION, WHICH INCLUDED A GEAR SWING, FOUND EXCESSIVE WEAR IN THE NOSE GEAR, CAUSING THE GEAR TO EASILY MOVE PAST THE OVER-CTR, MAKING IT POSSIBLE THAT A BUMP MAY HAVE FOLDED THE GEAR FORWARD. FAA INVESTIGATION CONCLUDED THAT MECHANICAL DEFECT WAS THE CAUSE OF THIS INCIDENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.