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Attributes | |
ACN | 552863 |
Time | |
Date | 200206 |
Day | Fri |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | msl single value : 41000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zzzz.artcc |
Operator | general aviation : corporate |
Make Model Name | IAI1125 (Astra) |
Operating Under FAR Part | Part 91 |
Navigation In Use | other |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : corporate |
Function | flight crew : first officer |
Qualification | pilot : multi engine pilot : instrument pilot : atp pilot : cfi |
Experience | flight time last 90 days : 71 flight time total : 6062 flight time type : 84 |
ASRS Report | 552863 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport flight crew : regained aircraft control |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft Weather |
Primary Problem | Aircraft |
Narrative:
We were eastbound at FL410 in cruise flight (center granted 'wrong way' altitude) with the autoplt on. The captain was preparing a cup of coffee as the autoplt began a series of uncommanded heading changes. I asked to hand fly the airplane and turned the autoplt off. I immediately realized that roll control was abnormal. The aileron control forces were very high and produced a 'sticky' or 'rachety' feel. I advised the captain and he took the controls, agreeing with me about the abnormal aileron situation. We asked for descent to fl 370 and reviewed procedures for this situation. The problem remained so we advised ATC that we wished to make a precautionary landing at ZZZ and were descended and vectored to do so. Passing into warmer air at about 15000 MSL the ailerons began to react normally and we made a normal landing. An out of specification aileron control rod lateral bearing was found and replaced. Also, the aircraft had sat in the rain at ZZZ1, first officer. The two previous days and there was some speculation that moisture may have reached into the system and frozen at altitude, although none was observed during the inspection. Callback conversation with reporter revealed the following information: the reporter stated the airplane was parked for two days in heavy rain and water had penetrated the wing leading edge where all the aileron control components were located. The reporter said the wing leading edge was found to be poorly sealed and required sealing work to prevent water soaking. The reporter stated a control rod bearing was out of limits and replaced and one aileron actuator was found rubbing on an access plate screw. The reporter said the actuator access plates have three different length fasteners and the one long screw was installed improperly. The reporter stated it is believed the main cause of the abnormal ailerons was freezing of the aileron components due to water penetration.
Original NASA ASRS Text
Title: A IAI1125 WESTWIND IN CRUISE AT FL410 DIVERTED DUE TO ABNORMAL AILERON CTL.
Narrative: WE WERE EASTBOUND AT FL410 IN CRUISE FLT (CENTER GRANTED 'WRONG WAY' ALTITUDE) WITH THE AUTOPLT ON. THE CAPT WAS PREPARING A CUP OF COFFEE AS THE AUTOPLT BEGAN A SERIES OF UNCOMMANDED HEADING CHANGES. I ASKED TO HAND FLY THE AIRPLANE AND TURNED THE AUTOPLT OFF. I IMMEDIATELY REALIZED THAT ROLL CTL WAS ABNORMAL. THE AILERON CTL FORCES WERE VERY HIGH AND PRODUCED A 'STICKY' OR 'RACHETY' FEEL. I ADVISED THE CAPT AND HE TOOK THE CTLS, AGREEING WITH ME ABOUT THE ABNORMAL AILERON SIT. WE ASKED FOR DSCNT TO FL 370 AND REVIEWED PROCS FOR THIS SIT. THE PROB REMAINED SO WE ADVISED ATC THAT WE WISHED TO MAKE A PRECAUTIONARY LNDG AT ZZZ AND WERE DSNDED AND VECTORED TO DO SO. PASSING INTO WARMER AIR AT ABOUT 15000 MSL THE AILERONS BEGAN TO REACT NORMALLY AND WE MADE A NORMAL LNDG. AN OUT OF SPECIFICATION AILERON CTL ROD LATERAL BEARING WAS FOUND AND REPLACED. ALSO, THE ACFT HAD SAT IN THE RAIN AT ZZZ1, FO. THE TWO PREVIOUS DAYS AND THERE WAS SOME SPECULATION THAT MOISTURE MAY HAVE REACHED INTO THE SYSTEM AND FROZEN AT ALTITUDE, ALTHOUGH NONE WAS OBSERVED DURING THE INSPECTION. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE AIRPLANE WAS PARKED FOR TWO DAYS IN HEAVY RAIN AND WATER HAD PENETRATED THE WING LEADING EDGE WHERE ALL THE AILERON CTL COMPONENTS WERE LOCATED. THE RPTR SAID THE WING LEADING EDGE WAS FOUND TO BE POORLY SEALED AND REQUIRED SEALING WORK TO PREVENT WATER SOAKING. THE RPTR STATED A CTL ROD BEARING WAS OUT OF LIMITS AND REPLACED AND ONE AILERON ACTUATOR WAS FOUND RUBBING ON AN ACCESS PLATE SCREW. THE RPTR SAID THE ACTUATOR ACCESS PLATES HAVE THREE DIFFERENT LENGTH FASTENERS AND THE ONE LONG SCREW WAS INSTALLED IMPROPERLY. THE RPTR STATED IT IS BELIEVED THE MAIN CAUSE OF THE ABNORMAL AILERONS WAS FREEZING OF THE AILERON COMPONENTS DUE TO WATER PENETRATION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.