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|
Attributes | |
ACN | 556386 |
Time | |
Date | 200208 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : lgb.airport |
State Reference | CA |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : sct.tracon |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 556386 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : pack mixing valve position indicator. pack temp. other flight crewa other flight crewb |
Resolutory Action | aircraft : equipment problem dissipated other |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Aircraft |
Narrative:
After departure from lgb, we discovered that the right temperature controller was stuck in the full cold position and would not work in either automatic or manual. After looking in both books and finding no procedure, we called maintenance to troubleshoot. They recommended pulling and resetting 3 circuit breakers. We tried this to no avail, and found with our heavy passenger load and keeping the left controller hotter than normal, it was bearable in the aft part of the jet. After leveling at cruise, I decided to turn on all the wing and engine anti-ice to see if this would do any good. Almost as soon as the wing anti-ice came on, the valve started working, leading me to believe that the pressure change unstuck the control valve. I think it would be a good idea to incorporate this procedure with the circuit breakers and anti-ice into our QRH book. Since it was a balmy morning in lgb, the valve, being in the full cold, worked for our cooling needs on the ground, so we never knew it wasn't working properly. Had it been a cold/frosty morning in winter with a valve stuck in the 1/2 - 3/4 position, we may have had to divert shortly after takeoff for an uncontrollable cabin temperature.
Original NASA ASRS Text
Title: MD80 CREW FOUND THE R PACK MIXING VALVE WAS STUCK IN THE COLD POS.
Narrative: AFTER DEP FROM LGB, WE DISCOVERED THAT THE R TEMP CONTROLLER WAS STUCK IN THE FULL COLD POS AND WOULD NOT WORK IN EITHER AUTO OR MANUAL. AFTER LOOKING IN BOTH BOOKS AND FINDING NO PROC, WE CALLED MAINT TO TROUBLESHOOT. THEY RECOMMENDED PULLING AND RESETTING 3 CIRCUIT BREAKERS. WE TRIED THIS TO NO AVAIL, AND FOUND WITH OUR HVY PAX LOAD AND KEEPING THE L CONTROLLER HOTTER THAN NORMAL, IT WAS BEARABLE IN THE AFT PART OF THE JET. AFTER LEVELING AT CRUISE, I DECIDED TO TURN ON ALL THE WING AND ENG ANTI-ICE TO SEE IF THIS WOULD DO ANY GOOD. ALMOST AS SOON AS THE WING ANTI-ICE CAME ON, THE VALVE STARTED WORKING, LEADING ME TO BELIEVE THAT THE PRESSURE CHANGE UNSTUCK THE CTL VALVE. I THINK IT WOULD BE A GOOD IDEA TO INCORPORATE THIS PROC WITH THE CIRCUIT BREAKERS AND ANTI-ICE INTO OUR QRH BOOK. SINCE IT WAS A BALMY MORNING IN LGB, THE VALVE, BEING IN THE FULL COLD, WORKED FOR OUR COOLING NEEDS ON THE GND, SO WE NEVER KNEW IT WASN'T WORKING PROPERLY. HAD IT BEEN A COLD/FROSTY MORNING IN WINTER WITH A VALVE STUCK IN THE 1/2 - 3/4 POS, WE MAY HAVE HAD TO DIVERT SHORTLY AFTER TKOF FOR AN UNCTLABLE CABIN TEMP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.