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|
Attributes | |
ACN | 562543 |
Time | |
Date | 200210 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Altitude | agl single value : 0 |
Aircraft 1 | |
Controlling Facilities | tower : oak.tower |
Operator | common carrier : air carrier |
Make Model Name | B757 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
ASRS Report | 562543 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : #2 egt indicator other flight crewa other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Takeoff on runway 36R at dfw in our B757 jet right close to V1 and bang, bang, bang. Hugely loud noises and vibrations shattered the plan to go flying. The captain and I threw a school-house perfect abort. CRM rules as we teamed with the cabin crew and returned to the gate with no injury or further incident. The lead mechanic reported that one of our #2 engines had a compressor stall. Callback conversation with reporter revealed the following information: the reporter stated the cause of the engine stalling and the high egt has not been reported by maintenance. The reporter said the engine was changed but no other details on component failure are known.
Original NASA ASRS Text
Title: A B757-200 ON TKOF ROLL JUST BELOW V1 REJECTED THE TKOF DUE TO #2 ENG COMPRESSOR STALLING AND HIGH EGT.
Narrative: TKOF ON RWY 36R AT DFW IN OUR B757 JET R CLOSE TO V1 AND BANG, BANG, BANG. HUGELY LOUD NOISES AND VIBRATIONS SHATTERED THE PLAN TO GO FLYING. THE CAPT AND I THREW A SCHOOL-HOUSE PERFECT ABORT. CRM RULES AS WE TEAMED WITH THE CABIN CREW AND RETURNED TO THE GATE WITH NO INJURY OR FURTHER INCIDENT. THE LEAD MECH RPTED THAT ONE OF OUR #2 ENGS HAD A COMPRESSOR STALL. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE CAUSE OF THE ENG STALLING AND THE HIGH EGT HAS NOT BEEN RPTED BY MAINT. THE RPTR SAID THE ENG WAS CHANGED BUT NO OTHER DETAILS ON COMPONENT FAILURE ARE KNOWN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.