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Attributes | |
ACN | 564536 |
Time | |
Date | 200210 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : den.airport |
State Reference | CO |
Altitude | agl single value : 0 |
Environment | |
Weather Elements | Ice Fog |
Aircraft 1 | |
Controlling Facilities | tower : atl.tower |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground other : eng runup |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 564536 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : less severe inflight encounter : weather inflight encounter other other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : vibration monitor other flight crewa other flight crewb |
Resolutory Action | other |
Consequence | other other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft Weather |
Primary Problem | Aircraft |
Narrative:
WX was IFR, temperature 18 degrees F, visibility 1 mi. After remote deiced, took runway 34 for takeoff. Performed engine runup on runway. Noticed initially #2 engine vibration higher than normal (3.0). After a few seconds, returned to more normal value (1.5). All other engine parameters completely normal. After runup, commenced takeoff and everything was normal until 10000 ft. #2 engine went above 4.0 on vibration. I suspected engine ice and performed ice shedding procedure (45% then to 80%) and ran high vibration irregular procedure for engine ice. Engine immediately returned to normal value (1.5). We continued to cruise and engine was normal until descent. On descent to phl, whenever engine thrust changed (retarded or advanced), vibration would go initially to around 3.0, then return again to 1.5 or so. Now wondered if we had something more than an ice problem, as no icing conditions existed into phl. Made a log entry and discussed with maintenance on arrival. Next day, found out engine had rotor blade warping. I believe we did everything correctly. Maybe should have retarded throttles to idle on runup and tried runup second time, but at time, did not seem necessary as engine vibration returned to normal value during runup.
Original NASA ASRS Text
Title: B737-300 CREW HAD SUSPECTED ENG FAN BLADE ICING THAT WAS DETECTED ON THE VIBRATION MONITOR.
Narrative: WX WAS IFR, TEMP 18 DEGS F, VISIBILITY 1 MI. AFTER REMOTE DEICED, TOOK RWY 34 FOR TKOF. PERFORMED ENG RUNUP ON RWY. NOTICED INITIALLY #2 ENG VIBRATION HIGHER THAN NORMAL (3.0). AFTER A FEW SECONDS, RETURNED TO MORE NORMAL VALUE (1.5). ALL OTHER ENG PARAMETERS COMPLETELY NORMAL. AFTER RUNUP, COMMENCED TKOF AND EVERYTHING WAS NORMAL UNTIL 10000 FT. #2 ENG WENT ABOVE 4.0 ON VIBRATION. I SUSPECTED ENG ICE AND PERFORMED ICE SHEDDING PROC (45% THEN TO 80%) AND RAN HIGH VIBRATION IRREGULAR PROC FOR ENG ICE. ENG IMMEDIATELY RETURNED TO NORMAL VALUE (1.5). WE CONTINUED TO CRUISE AND ENG WAS NORMAL UNTIL DSCNT. ON DSCNT TO PHL, WHENEVER ENG THRUST CHANGED (RETARDED OR ADVANCED), VIBRATION WOULD GO INITIALLY TO AROUND 3.0, THEN RETURN AGAIN TO 1.5 OR SO. NOW WONDERED IF WE HAD SOMETHING MORE THAN AN ICE PROB, AS NO ICING CONDITIONS EXISTED INTO PHL. MADE A LOG ENTRY AND DISCUSSED WITH MAINT ON ARR. NEXT DAY, FOUND OUT ENG HAD ROTOR BLADE WARPING. I BELIEVE WE DID EVERYTHING CORRECTLY. MAYBE SHOULD HAVE RETARDED THROTTLES TO IDLE ON RUNUP AND TRIED RUNUP SECOND TIME, BUT AT TIME, DID NOT SEEM NECESSARY AS ENG VIBRATION RETURNED TO NORMAL VALUE DURING RUNUP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.