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|
Attributes | |
ACN | 567288 |
Time | |
Date | 200212 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : geg.airport |
State Reference | WA |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | IMC |
Weather Elements | Fog Ice |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Dash 8-400 |
Operating Under FAR Part | Part 121 |
Flight Phase | landing : roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : commercial pilot : instrument pilot : multi engine |
Experience | flight time last 90 days : 210 flight time total : 2500 flight time type : 500 |
ASRS Report | 567288 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | excursion : runway inflight encounter : weather non adherence : company policies non adherence : far non adherence : published procedure other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Airport |
Primary Problem | Flight Crew Human Performance |
Narrative:
Expected a captain-monitored ILS runway 3 to geg. Normal approach with the captain landing the airplane. Normal deceleration until the captain braked to turn off the runway. Braking had no effect and the antiskid system started working. We slid past the threshold and about 200 ft into the overrun. Minimal aircraft damage and the passenger deplaned normally. I think that 2 things caused this incident. First, the latest metar we had showed that braking action was good. Tower didn't state otherwise. In fact, it wasn't good. I would estimate that it was probably fair with some areas of poor. Second, I feel that our brakes should've been more effective. Even though braking action was less than good, there was just a little frost on the runway and we should've been able to stop in the distance we had remaining. To prevent this from happening again, the aircraft should be fitted with better brakes and the tower should solicit and give out braking action reports.
Original NASA ASRS Text
Title: A DHC-8-400 CREW SLID 200 FT INTO THE OVERRUN OF RWY 3 AFTER LNDG FROM AN ILS.
Narrative: EXPECTED A CAPT-MONITORED ILS RWY 3 TO GEG. NORMAL APCH WITH THE CAPT LNDG THE AIRPLANE. NORMAL DECELERATION UNTIL THE CAPT BRAKED TO TURN OFF THE RWY. BRAKING HAD NO EFFECT AND THE ANTISKID SYS STARTED WORKING. WE SLID PAST THE THRESHOLD AND ABOUT 200 FT INTO THE OVERRUN. MINIMAL ACFT DAMAGE AND THE PAX DEPLANED NORMALLY. I THINK THAT 2 THINGS CAUSED THIS INCIDENT. FIRST, THE LATEST METAR WE HAD SHOWED THAT BRAKING ACTION WAS GOOD. TWR DIDN'T STATE OTHERWISE. IN FACT, IT WASN'T GOOD. I WOULD ESTIMATE THAT IT WAS PROBABLY FAIR WITH SOME AREAS OF POOR. SECOND, I FEEL THAT OUR BRAKES SHOULD'VE BEEN MORE EFFECTIVE. EVEN THOUGH BRAKING ACTION WAS LESS THAN GOOD, THERE WAS JUST A LITTLE FROST ON THE RWY AND WE SHOULD'VE BEEN ABLE TO STOP IN THE DISTANCE WE HAD REMAINING. TO PREVENT THIS FROM HAPPENING AGAIN, THE ACFT SHOULD BE FITTED WITH BETTER BRAKES AND THE TWR SHOULD SOLICIT AND GIVE OUT BRAKING ACTION RPTS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.