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|
Attributes | |
ACN | 572216 |
Time | |
Date | 200301 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : fme.airport |
State Reference | MD |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : pct.tracon tower : sequ.tower |
Operator | general aviation : personal |
Make Model Name | PA-28 Cherokee/Archer II/Dakota/Pillan/Warrior |
Operating Under FAR Part | Part 91 |
Navigation In Use | other |
Flight Phase | descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : private pilot : instrument |
Experience | flight time last 90 days : 30 flight time total : 2300 flight time type : 2100 |
ASRS Report | 572216 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Events | |
Anomaly | non adherence : far |
Independent Detector | other flight crewa |
Resolutory Action | none taken : anomaly accepted none taken : detected after the fact |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft |
Primary Problem | Flight Crew Human Performance |
Narrative:
I was approaching fort meade, md, runway 28 in my piper 180 when my engine lost all power though the propeller continued to windmill. I was about 3 mi from the end of the runway and in a descent. I had just canceled my IFR plan with baltimore and had switched to the fort meade unicom. I immediately switched back to baltimore to advise my situation. After I gained the runway, I let baltimore know all was ok. He acknowledged. Later I called FSS to make sure baltimore knew the outcome. The evident reason for the engine out was a lack of fuel in the left tank. I was completing my landing check when the problem occurred, and there was no time to finish. The engine fired up after a touchdown bump in the field before the runway which permitted a normal landing. The evident reason for the fuel problem was a recent overhaul which reduced the time on each tank from 2 1/2 hours to 2. I was aware of this and was still using mineral oil. Since the flight took 3 hours from connecticut, there would have been 1 hour left in the right tank. Having not completed my landing check due to the problem, I did not know that. The solution is to start landing checks earlier, probably before descent. Obviously this mistake will not be repeated.
Original NASA ASRS Text
Title: PIPER 180 PLT HAS FUEL STARVATION DURING APCH TO FME.
Narrative: I WAS APCHING FORT MEADE, MD, RWY 28 IN MY PIPER 180 WHEN MY ENG LOST ALL PWR THOUGH THE PROP CONTINUED TO WINDMILL. I WAS ABOUT 3 MI FROM THE END OF THE RWY AND IN A DSCNT. I HAD JUST CANCELED MY IFR PLAN WITH BALTIMORE AND HAD SWITCHED TO THE FORT MEADE UNICOM. I IMMEDIATELY SWITCHED BACK TO BALTIMORE TO ADVISE MY SIT. AFTER I GAINED THE RWY, I LET BALTIMORE KNOW ALL WAS OK. HE ACKNOWLEDGED. LATER I CALLED FSS TO MAKE SURE BALTIMORE KNEW THE OUTCOME. THE EVIDENT REASON FOR THE ENG OUT WAS A LACK OF FUEL IN THE L TANK. I WAS COMPLETING MY LNDG CHK WHEN THE PROB OCCURRED, AND THERE WAS NO TIME TO FINISH. THE ENG FIRED UP AFTER A TOUCHDOWN BUMP IN THE FIELD BEFORE THE RWY WHICH PERMITTED A NORMAL LNDG. THE EVIDENT REASON FOR THE FUEL PROB WAS A RECENT OVERHAUL WHICH REDUCED THE TIME ON EACH TANK FROM 2 1/2 HRS TO 2. I WAS AWARE OF THIS AND WAS STILL USING MINERAL OIL. SINCE THE FLT TOOK 3 HRS FROM CONNECTICUT, THERE WOULD HAVE BEEN 1 HR LEFT IN THE R TANK. HAVING NOT COMPLETED MY LNDG CHK DUE TO THE PROB, I DID NOT KNOW THAT. THE SOLUTION IS TO START LNDG CHKS EARLIER, PROBABLY BEFORE DSCNT. OBVIOUSLY THIS MISTAKE WILL NOT BE REPEATED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.