Narrative:

Following a normal start and taxi through the takeoff run, experienced a tail strike during a liftoff from the runway. Winds at the time were 090 degrees at 9 KTS (ATIS). Winds seemed gusty during takeoff roll. Rotation rate seemed to start out normally but increased slightly at liftoff with no additional force applied. I heard a muffled noise at the same time. Shortly after takeoff, the flight attendant called forward to say she thought she had heard a noise and also thought the tail had hit the ground. While the captain coordinated completion of the abnormal procedure with the company (maintenance), I coordinated with ATC to return to dfw. Return flight and landing were uneventful. Maintenance inspection revealed scraped paint on tailskid but noted no other damage to tailskid unit. Aircraft was inspected in accordance with maintenance procedures, released for flight and re-dispatched to slc. During following takeoff, captain noted the nose seemed to want to rotate faster than normal. Postflt load audit was conducted and revealed cargo was 500 pounds heavier than indicated. Maintenance results of stabilizer inspection are pending.

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Original NASA ASRS Text

Title: TAIL STRIKE IN A B737-800 DURING A ROTATION RATE THAT APPEARED TO INCREASE SLIGHTLY AT TKOF AT DFW, TX.

Narrative: FOLLOWING A NORMAL START AND TAXI THROUGH THE TKOF RUN, EXPERIENCED A TAIL STRIKE DURING A LIFTOFF FROM THE RWY. WINDS AT THE TIME WERE 090 DEGS AT 9 KTS (ATIS). WINDS SEEMED GUSTY DURING TKOF ROLL. ROTATION RATE SEEMED TO START OUT NORMALLY BUT INCREASED SLIGHTLY AT LIFTOFF WITH NO ADDITIONAL FORCE APPLIED. I HEARD A MUFFLED NOISE AT THE SAME TIME. SHORTLY AFTER TKOF, THE FLT ATTENDANT CALLED FORWARD TO SAY SHE THOUGHT SHE HAD HEARD A NOISE AND ALSO THOUGHT THE TAIL HAD HIT THE GND. WHILE THE CAPT COORDINATED COMPLETION OF THE ABNORMAL PROC WITH THE COMPANY (MAINT), I COORDINATED WITH ATC TO RETURN TO DFW. RETURN FLT AND LNDG WERE UNEVENTFUL. MAINT INSPECTION REVEALED SCRAPED PAINT ON TAILSKID BUT NOTED NO OTHER DAMAGE TO TAILSKID UNIT. ACFT WAS INSPECTED IN ACCORDANCE WITH MAINT PROCS, RELEASED FOR FLT AND RE-DISPATCHED TO SLC. DURING FOLLOWING TKOF, CAPT NOTED THE NOSE SEEMED TO WANT TO ROTATE FASTER THAN NORMAL. POSTFLT LOAD AUDIT WAS CONDUCTED AND REVEALED CARGO WAS 500 LBS HEAVIER THAN INDICATED. MAINT RESULTS OF STABILIZER INSPECTION ARE PENDING.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.